IFA Accident Reports
Safe flying is the aim of all pilots and comes
from training and experience. These accidents reports
are presented in the interest of safety by helping
pilots learn from the experience of others. To view
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and Maneuvering Accidents
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Where: Grayslake, IL
Injuries: None
Phase of Flight: Landing
The single-engine airplane veered off the left
side of runway 9 (3,270 feet by 40 feet, asphalt)
during landing and sustained substantial damage.
Winds, 11 miles from the accident airport, were
120 degrees at 11 knots gusting to 21 knots. The
pilot reported that he flew a Global Positioning
System (GPS) approach and cancelled his instrument
flight rules (IFR) flight plan when he had the airport
in sight. He entered a left downwind for landing
on runway 9 and confirmed a right crosswind condition
by observing the windsock. The airspeed was 90 knots
with a right "crab" on final approach to landing.
The pilot reported, "Prior to touchdown the wind
calmed to the point that the crab was not needed."
He reported the airplane touched down on the centerline
of the dry runway. He reported, "Almost immediately
after touchdown, the plane started moving left."
He reacted by putting in full right aileron and
applying right rudder, but he did not apply any
pressure to the toe brakes. The airplane veered
off the left side of the runway. The airplane encountered
soft terrain, spun around, and impacted a ditch.
The inspection of the airplane revealed that the
wheels spun freely when turned and the brakes did
not stick. The tires had no flat spots. The inspection
of the runway revealed that there were no long skid
marks on the runway, but there were black skid marks
about 2 feet in length that were about 20 feet apart.
There was no indication of braking when the airplane
came in contact with the grass.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot failed to compensate adequately for the
crosswind condition and failed to maintain directional
control during the landing roll. Contributing factors
included the crosswind, the narrow runway, soft
ground, and the ditch.
Source: National Transportation Board
Aircraft: Aeronca 7AC
Where: Novato, CA
Injuries: None
Phase of flight: Cruising
The pilot reported that while in cruise flight, the engine suddenly started running rough and the engine rpms rapidly decreased from 2,100 to 1,900. The pilot immediately applied full carburetor heat, but the engine continued running rough so he headed toward the nearest airport. While on the base leg of the traffic pattern, the engine lost all power. The airplane subsequently touched down short of the runway and collided with a fence. Post-accident examination of the wreckage found that the left auxiliary fuel tank was empty and the right auxiliary tank was about one-third full. The auxiliary tank fuel selector under the instrument panel was found in the off position. The main fuel tank, which was configured to feed the engine, was full and the fuel indicator also indicated full. Further examination of the engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.
The pilot reported that the main fuel tank fuel cap was misplaced when the airplane was refueled. The pilot then borrowed a fuel cap from a local mechanic and installed it on the main tank filler port. An examination of the airplane revealed that the borrowed fuel cap was a non-vented type; because there was no other vent for the main tank, the only vent would be through a vented cap. As fuel was used from the main tank, the lack of a vented cap caused a vacuum within the main tank that eventually reduced the fuel flow, starving the engine. Had an auxiliary tank been selected, adequate venting would have occurred because both auxiliary tanks had vented fuel caps.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's use of a non-vented fuel cap, which resulted in a total loss of engine power due to fuel starvation.
Source: National Transportation Board
Aircraft: Cirrus SR 2
Where: Edgewater, MD
Injuries: 1 fatal
Phase of Flight: Landing
A Cirrus SR-22 was destroyed when it impacted a tree and terrain during a go-around after an attempted landing at the Lee Airport (ANP), Edgewater, Maryland. The private pilot initially survived the accident and was taken to a hospital, but died about three weeks later as a result of the injuries sustained during the accident. The 14 Code of Federal Regulations Part 91 personal flight departed the Ocean City Municipal Airport (26N), Ocean City, New Jersey, with ANP as the final destination. Visual meteorological conditions prevailed at the time of the accident. An instrument flight rules (IFR) flight plan had been filed.
A witness reported that he observed the airplane enter the airport's landing pattern by entering a 45-degree entry from the northeast. The witness reported that the airplane crossed runway 30 about mid-field and entered a left downwind leg for landing on runway 30.
Another witness, who was standing on the ramp of the maintenance hangar at ANP, reported that he heard the pilot make a radio call over the airport's Unicom frequency stating that he was landing on runway 30. The witness reported that he observed the airplane over the approach end of the runway at an altitude of 150 - 175 feet above ground level (agl). He reported that the airplane was "diving for the runway" and was flying on the left side of the runway over the grass between the taxiway and the runway. The airplane continued to "dive" until it was about one half way down the runway when the nose of the airplane leveled out at an altitude of about 75 feet agl. He heard the engine noise increase, but not to full power. He reported that the airplane "banked hard to the left" and that he could see the top of both wings. He lost sight of the airplane behind a line of trees, and later heard a "thud" followed by another thud.
The same witness reported that the airplane's engine sounded normal with no backfiring or sputtering. He heard a slight increase of engine power when the nose of the airplane leveled out. He reported that the flaps were partially extended.
A third witness, who was working in his hangar located about mid-field at the airport, reported that he heard the airplane when it was over the runway. He reported that the airplane sounded like it was "not developing a lot of power" but was "coasting." Then the airplane powered up "a little bit" and then turned to the left. The witness reported that he did not see the airplane after the turn, but he heard the engine "miss" or "stop" when it was over the neighborhood. The witness ran to the accident site when he heard the crash.
Two construction workers, who were working on a house on Lee's Lane which was located about 1/8 of a mile from the accident site, reported that they heard the airplane as it flew over the house. They described the engine noise as being "extremely loud" prior to the sound of the airplane impacting the trees.
Numerous witnesses arrived at the accident site located about 100 yards from the third witness's hangar. Fuel was spilling from both fuel tanks. They removed the seat belt and shoulder harness from the pilot and pulled him from the airplane. An emergency medical helicopter arrived at the scene and the pilot was flown to a hospital.
The pilot held a private pilot certificate with single-engine land and instrument ratings. He held a third-class medical certificate with the following restriction: "Must wear corrective lenses for near and distant vision." The pilot had a total of 2,746 flight hours. The pilot had received 9.5 hours of initial flight training in the Cirrus SR-22, through the Cirrus Design flight-training program in Duluth, Minnesota. He had a total of 167 hours in the SR-22.
AIRCRAFT INFORMATION
The airplane was a Cirrus SR-22 manufactured in 2003. The airplane seated four and had a maximum gross weight of 3,400 pounds. The engine was a 310 horsepower Continental IO-550-N engine. The airplane had flown approximately 3.8 hours since the last inspection and had a total time of 391 hours.
METEOROLOGICAL CONDITIONS
At 0954, the observed surface weather at BWI (Baltimore/Washington International) located about 14 nautical miles north northwest of ANP, was: winds 220 degrees at 7 kts, visibility 4 statute miles, haze, temperature 28 degrees Celsius (C), dew point 22 degrees C, altimeter 30.11 inches of mercury.
WRECKAGE AND IMPACT INFORMATION
The airplane impacted an oak tree about 75 feet in height that was located in a residential neighborhood that bordered the airport property. The airplane wreckage was found in a soybean field that was on the airport property. The oak tree exhibited strikes at the top of the tree and three large tree limbs were knocked down in a northerly direction. The same oak tree also had tree limbs that did not exhibit any damage located to the right and left of the three large limbs that were knocked down. The airplane's initial point of impact on the ground was about 30 feet from the oak tree on a magnetic heading of 060 degrees. The descent angle from the oak tree to the initial impact point was about 35 - 40 degrees.
Numerous branches were in the wreckage path between the oak tree and the main wreckage. The initial ground impact point exhibited a slash through the black dirt that was about 56 inches wide and was consistent with a propeller strike. There was a depression in the ground that was about 5 feet in length at the initial impact point going toward the main wreckage.
The main wreckage was located about 65 feet from the oak tree. The longitudinal axis of the wreckage was on a 240 magnetic heading. The engine was found on the right wing of the aircraft next to the cabin, facing aft. The engine remained attached to the firewall via control cables and hoses. The nose landing gear was separated from the fuselage and was found near the main wreckage.
The belly and floor of the cockpit forward of the spar tunnel were pushed upwards. The firewall and cockpit instrument panel were pushed back into the cockpit and were over both front seat bottom cushions. The pilot's seatbelt was found open but intact. The flap switch was found in the 100% (full down) setting. The fuel selector was set to the right tank.
The left inboard wing section remained attached to the fuselage and exhibited forward edge buckling. The wing root area from the fuselage outboard to the fresh air inlet was missing pieces of wing skin. The hole left by the missing pieces of skin contained tree leaves consistent with the trees the aircraft struck during the impact sequence. The main spar exhibited multiple delaminations along its length. The left flap was separated from one of its hinge points. The left flap outward of the mid-span hinge buckled in two places and was bent upward. The inboard trailing edge of the flap was buckled forward. A measurement was taken from the inboard side of the left flap from the forward side of the anti-scuff tape to the wing cove. The distance measured was approximately 4 inches. The left main landing gear remained attached to the left wing, but was bent to the left.
The outboard section of the left wing was broken off during the impact sequence at approximately wing station (WS) 132. The outboard section of the left wing, which included about a 3-foot section of wing, the left aileron, the left wingtip, and the left strobe, were found in the residential yards that were located south of the oak tree.
The right inboard wing remained attached to the fuselage and exhibited forward edge buckling and had large jagged cuts with missing sections of wing skin. The main spar exhibited multiple delaminations along its length. The flap on the right wing separated from two of its three hinge points. The flap was torn and dented along the leading edge with a large upward buckle just outboard of the mid-span hinge. The outboard section of the right wing was broken at wing station (WS) 132, but it remained attached to the wing and was found with the main wreckage. The right wingtip was found with the main wreckage. The right main landing gear was separated from the right wing and was found with the main wreckage. It exhibited bending to the left.
The empennage separated from the fuselage just forward of the fuselage station (FS) 289 bulkhead, but it remained attached by the rudder and elevator cables. The horizontal stabilizer was found mostly intact. Both elevators showed impact damage. The damage to the right elevator was concentrated at the tip. The elevator buckled at the outboard end. The left elevator showed buckling on the trailing edge side in two places. The left elevator could not be moved up or downward from having been forced forward into the horizontal stabilizer. The vertical stabilizer had damage to the leading edge on the topside of the empennage. The rudder separated from the vertical stabilizer and was found lying across the left horizontal stabilizer.
Flight control cable continuity was checked. All cables were traced from the flight controls to their respective attach points on the flight control surfaces. There were no cable breaks to any of the flight control cables.
The roll and pitch trim actuators were found in approximately the neutral setting. The flap actuator arm had sheared from the motor housing of the flap actuator but remained attached to the flap torque tube assembly. The flap actuator arm protruded approximately 1/4 inch from its housing which is consistent with a flap setting of 100% (full down).
The Cirrus Airframe Parachute System (CAPS) system was found un-deployed. The parachute enclosure cover was found separated from the aircraft about 10 feet to the left side of the empennage. The activation cable was examined and the CAPS safety pin was found stowed in the handle and handle holder assembly. The CAPS system was rendered safe on site by cutting the activation cable at the fuselage station (FS) 222 bulkhead. The components that could pose a danger to personnel were removed and detonated or burned.
A fuel sample was taken from the left wing as the airplane was recovered. The fuel sample was light blue in color with no apparent contamination.
The engine inspection revealed that the crankcase was intact and undamaged. The crankshaft rotated freely and engine drive and valve train continuity was established. "Thumb" compression was obtained on all cylinders. The magnetos remained attached to the engine and were undamaged. The left and right magneto mounting flanges exhibited mechanical/rotational signatures (approx. 3 mm) on both sides of the mounting plates (paint scraped away). The left and right magnetos impulse couplings engaged when the crankshaft was rotated. The ignition harness was intact and a spark was emitted in conjunction with the impulse coupling actuation from all the upper spark plug leads. The spark plug electrodes exhibited normal operational signatures. The cylinders were examined with a borescope. No anomalies were observed to the cylinder walls, pistons, or valves. The left and right magneto-to-engine timing was checked using the timing markings on the crankshaft and found to be 22 degrees. The fuel pump drive coupling was intact and the pump rotated. The fuel pump, fuel manifold valve, and the throttle valve were sent to engine manufacturer for testing.
The propeller remained attached to the crankshaft propeller-mounting flange. The flange appeared undamaged. The propeller spinner exhibited aft crushing. All three-propeller blades remained attached to the propeller hub. The propeller and propeller governor were shipped to the propeller manufacturer for inspection.
TESTS AND RESEARCH
The MFD compact flash card was sent to Cirrus Design for downloading by Avidyne Corporation technicians with a Federal Aviation Administration inspector providing oversight. The download of the compact flash card indicated that the last flight recorded by the MFD was conducted on October 29, 2005. The data concerning the accident flight was not recorded due to memory size, or was deleted during the "power-up" of the MFD when the download was conducted.
The MFD compact flash card was sent to the Vehicle Recorders Division of the National Transportation Safety Board for inspection. The inspection confirmed that no information concerning the accident flight was found on the compact flash card.
The fuel system components were bench tested at Teledyne Continental Motors (TCM) , with National Transportation Safety Board (NTSB) providing oversight. The bench test of the fuel pump and fuel manifold valve indicated that they functioned through their full range of operation. The throttle and metering assembly was intact and undamaged. The TCM report stated that the first flow test cycle yielded values outside the TCM specifications. A second test cycle was accomplished where the assembly was adjusted to verify its ability to flow within TCM calibration specifications. Adjustments to the idle speed and mixture adjustments produced fuel flows within TCM calibration specifications. The TCM report stated, "During all test phases, the assembly functioned properly through its full range of operation."
The TCM report stated the following:
"The 'Observed' fuel flows and/or pressures are recorded without adjustment (unless noted) of the fuel system component. ... These tests and adjustments are carried out in an environment of controlled fuel supply pressures and calibrated test equipment.
When engines are installed in aircraft, they are subjected to a different induction system, fuel supply system and operating environment and may require further adjustments to compensate for these differences. It is these differences that may be present in the following test bench recorded values and TCM flow/pressure specifications. These tests are conducted to confirm that the fuel system components function adequately within its' design limitations."
A propeller teardown inspection of the McCauley propeller, model D3A34C443-A, was conducted at the McCauley Propeller facility at Wichita, Kansas. The NTSB investigator-in-charge (IIC) provided oversight of the inspection. The inspection of the propeller revealed that all three blades were still installed in the hub. The retaining ring attachment and shim packs were all dislodged and the blades were loose. All three blades exhibited normal leading edge burnishing and paint erosion, but there were no significant leading edge gouges. The number 1 blade (marked blade C on-site) was straight and undamaged out to the tip. The tip had a rearward bend. The chamber side of the blade had chordwise scoring in the white paint. The actuating pin was broken by impact damage. The number 2 blade (marked blade A on-site) had a forward bend at approximately the 12 to 14-inch station. The blade was then straight outboard with decreased pitch twist, and the last ten inches had tip damage. The actuating pin was intact. The number 3 blade (marked blade B on-site) had an aft bend at approximately 16 to 18-inch station. The rest of the blade was straight. The actuating pin was intact. The blade angle at impact was not determined due to impact damage.
The McCauley propeller governor model was inspected. The governor top cover was broken and the control shaft and control lever had received impact damage. The teardown of the governor indicated that the internal parts were intact and exhibited no damage.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's failure to maintain sufficient airspeed which resulted in a stall. A factor was the pilot’s failure to properly set the flaps for the go-around.
Aircraft: Cirrus SR20
Where: New York City
Injuries: 2 fatal
Phase of flight: Maneuvering
On October 11, 2006, about 1442 eastern daylight time, a Cirrus Design SR20, operated as a personal flight, crashed into an apartment building in Manhattan, New York City, while attempting to maneuver above the East River. The two pilots on board the airplane, a certificated private pilot who was the owner of the airplane and a passenger who was a certificated commercial pilot with a flight instructor certificate, were killed. One person on the ground sustained serious injuries, two persons on the ground sustained minor injuries, and the airplane was destroyed by impact forces and postcrash fire. The flight was operating under the provisions of 14 Code of Federal Regulations (CFR) Part 91, and no flight plan was filed. Marginal visual flight rules (MVFR) conditions prevailed at the time of the accident.
The accident airplane departed Teterboro Airport (TEB), Teterboro, New Jersey, about 1429 and was cleared for a visual flight rules (VFR) departure. According to air traffic control (ATC) transcripts, the pilots acknowledged that they were to stay out of the New York class B airspace. After takeoff, the accident airplane turned southeast and climbed to an altitude of about 600 to 800 feet. When the flight reached the western shore of the Hudson River, it turned to the south, remaining over the river, then descended to 500 feet. The flight continued southbound over the Hudson River until abeam of the southern tip of Manhattan, at which point the flight turned southwest bound. Radar data from John F. Kennedy International Airport (JFK), Jamaica, New York; Newark International Airport (EWR), Newark, New Jersey; and Westchester County Airport (HPN), White Plains, New York, indicated that the accident airplane’s altitude varied from 500 to 700 feet for the remainder of the flight.
About 1436, the airplane flew around the Statue of Liberty, then headed to the northeast, at which point, it proceeded to fly over the East River. About 1 mile north of the Queensboro Bridge, the airplane made a left turn to reverse its course. Radar contact was lost about 1442. The airplane impacted a 520-foot tall apartment building, 333 feet above street level.
This accident occurred in a complex section of airspace surrounding Manhattan Island, near three major air carrier airports and a variety of other general aviation facilities accommodating both fixed-wing and rotary-wing aircraft. Because of the high density of air traffic in this area, the FAA has designated most of the airspace “class B,” the second most restrictive designation for airspace in the United States.
The airplane impacted the 32nd and the 33rd floors of the north face of an apartment building located on 72nd Street. The engine, propeller, the right portion of the engine mount, and the nose landing gear strut were found in an apartment on the 32nd floor. The engine was found inverted with the propeller separated. The engine and propeller exhibited thermal damage and were coated with ash, debris, and fire-extinguishing agent.
The majority of the wreckage was on the street level at East 72nd Street, directly below the impact point. The wreckage was destroyed by impact forces and postcrash fire. Some wreckage debris was found on adjacent rooftops, balconies, and building projections. The examination of the wreckage indicated that there was no sign of an in-flight fire or any preexisting damage to the airplane.
VFR operations are authorized below the class B airspace surrounding Manhattan Island in designated zones called the Hudson River and East River exclusion areas. The FAA stated that the purpose of the Hudson and East River exclusion areas was to provide for VFR aircraft operations over the rivers for transiting, landing, or departing aircraft. Before the exclusion areas were defined, the floor of the class B airspace was typically at the surface of the rivers in the current areas of exclusion, and any aircraft operations over the rivers in these areas had to be coordinated with ATC. Seaplane and helicopter bases are currently located in or near these exclusion areas, and aircraft also use the Hudson River exclusion area to transit under the class B airspace.
The last communication between ATC and the accident flight was about 1433 when the accident pilots acknowledged that they were to squawk VFR. No further ATC communication was required while the flight was conducted in the Hudson and East River class B exclusion areas. Pilots are advised to announce their position and intentions on common traffic advisory frequency (CTAF) 123.05 Mhz when operating in the Hudson River exclusion area and CTAF 123.075 Mhz when operating in the East River exclusion area, but the announcements are not mandatory. There were no reports of the accident flight communicating on either of these frequencies. Pilots are also responsible for maintaining their own traffic separation
The airplane’s pilot/owner, age 34, held a private pilot certificate with a rating for airplane single engine land. His most recent Federal Aviation Administration (FAA) third-class medical certificate had no waivers or limitations. A review of his FAA airman file and medical records did not reveal any discrepancies or enforcement actions or preexisting medical conditions. He purchased the accident airplane on June 9, 2006.
According to the pilot/owner’s logbook at the time of the accident, he had accumulated 87.8 hours total flight time, all of which were accumulated in the last 12 months prior to the accident, including 12.5 hours in Cirrus aircraft, 3.9 hours of which were as pilot-in-command (PIC). In the last 90 days, 30 days and 24 hours before the accident flight, he flew 13.7 hours.
There were no system, structural, or engine malfunctions found. The engine was producing power as indicated by the separation of the propeller hub, damage to the blade hubs, and damage to the No. 2 blade. The pilot/owner was properly certificated to fly the accident airplane. The pilot-rated passenger was also a certified flight instructor and qualified to have flown the accident flight.
The National Transportation Safety Board determined that the probable cause of this accident was the pilots’ inadequate planning, judgment, and airmanship in the performance of a 180º turn maneuver inside of a limited turning space.
Source: National Transportation Board
Aircraft: Cirrus SR22
Where: Burnsville, NC
Injuries: None
Phase of flight: Landing
The pilot reported that he was low on the final approach to runway 32 at the mountaintop airport, but thought he could "make the numbers." The airplane encountered a downdraft, and the pilot wasn't able to compensate for it. The airplane impacted terrain about 3 feet short of the runway, bounced, then veered off the right side of the runway and struck an embankment, resulting in substantial damage to the right wing and fuselage. The pilot also stated that there was a 7-knot tailwind "from the right," and that the density altitude was about 6,300 feet at the time of the accident. The flight was the pilot’s seventh arrival into the airport, and his first time landing there with a tailwind. There were no pre-accident mechanical anomalies noted with the airplane, which "was performing great."
According to the airport's pilot manual, runway 32 was the preferred landing runway due to its upslope and fewer obstructions at the arrival end. There was no displaced threshold, and the terrain rose sharply to the approach end of the runway. A visual glideslope indicator was located to the left of the runway. The pilot's manual also advised, "consider flying a steeper approach to compensate for the 'burble' downdraft typically present at the end of the runway," and noted that the hills on either side and the runway's upslope "will combine to produce the optical illusion of being too steep an approach path." The manual further stated, "consider carefully the effects of density altitude on the performance of your aircraft," as well as, "many pilots will not consider landing with SSE winds, and will simply divert" to another airport.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's failure to maintain a proper visual glideslope during final approach.
Source: National Transportation Board
Aircraft:
Dassault Aviation DA-20 Falcon Jet
Where: Pueblo, CO
Injuries: 5 Uninjured.
Phase of flight: Landing
The captain reported that he obtained weather
briefings prior to and during the flight. The briefings
did not include any NOTAMS indicating a contaminated
runway at their destination airport. The captain
obtained a report from the local fixed base operator
that a Learjet had landed earlier and reported the
runway as being okay. The tower was closed on their
arrival, so they made a low pass over the airport
to inspect the runways. Based on the runway and
wind conditions, they decided their best choice
for landing was on runway 08L. The captain said
the landing was normal and the airplane initially
decelerated with normal braking. As they encountered
snow and ice patches, the captain said he elected
to deploy the thrust reversers. The captain said
that as the thrust reversers deployed, the airplane
began to yaw to the left and differential braking
failed to realign the airplane with the runway.
The captain said the airplane departed the left
side of the runway and rotated counter clockwise
before coming to rest on a southwesterly heading.
A witness on the airport said, "I watched them touch
down. I heard the [thrust] reversers go on and then
off, and then on again. As they came back on for
the second time, that s when the plane started making
full circles on the runway. This happened two, maybe
three times before going off the side of the runway."
The airplane s right main landing gear collapsed
on departing the runway, causing substantial damage
to the right wing, right main landing gear and aft
pressure bulkhead. At the accident site, the right
engine thrust reverser was partially deployed. The
left engine thrust reverser was fully deployed with
the blocker doors extended. An examination of the
airplane revealed a stuck solenoid on the right
engine thrust reverser. No other system anomalies
were found. Approximately 33 minutes prior to the
accident, the pilot requested from Denver Air Route
Traffic Control Center, the weather for the airport.
Denver Center reported the conditions as "winds
calm, visibility 6 miles with light mist, 3,000
overcast, temperature zero degrees Centigrade (C)
dew point -1 degree C, altimeter three zero 30.20,
and there was at least a half inch of slush on all
surfaces." The pilot acknowledged the information.
The NOTAM log for the airport showed that at 2115,
the airport issued a NOTAM stating there was "1/2
inch wet snow all surfaces." The airport operations
manager reported that at the time of the accident
the runway surface was covered with 3/4 inch of
wet snow. The airport conducts a 24 hour, 7 days
a week operation; however, operations support digresses
to fire coverage only after 2300.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s improper in-flight planning/decision
to land on the contaminated runway, the stuck thrust
reverser solenoid resulting in partial deployment
of the right engine thrust reverser, and the pilot
s inability to maintain directional control of the
airplane due to the asymmetric thrust combined with
a contaminated runway. Factors contributing to the
accident were the wet, snow-covered runway, the
airport s failure to remove the snow from the runway,
and the pilot s failure to recognize the reported
hazardous runway conditions by air traffic control.
Source: National Transportation Board
Aircraft: De
Havilland DHC-6
Where: Rittman, OH
Injuries: 1 serious,
one minor
Phase of Flight: Landing
A de Havilland DHC-6 was substantially damaged
when it impacted terrain following an aborted landing
at Hilty Field (OI68), Rittman, Ohio. The certificated
airline transport pilot received serious injuries,
and the second pilot, also a certificated airline
transport pilot, received minor injuries. Visual
meteorological conditions prevailed, and no flight
plan was filed for the parachuting flight.
During a telephone interview, the second pilot
stated that the purpose of the flight was to perform
an evaluation of the first pilot, who was recently
designated by the operator as a backup pilot.
The pilots initially departed and performed three
takeoff and landings, with the first pilot in the
right seat. They then embarked passengers, and performed
several parachuting flights. The pilots then decided
that the first pilot would transition to the left
seat. Two additional parachuting flights followed
uneventfully.
Following the passenger drop on the third flight,
the pilots discussed single engine operations. The
first pilot subsequently reduced the right engine
s power to flight idle, and feathered the propeller.
During the final leg of the approach to landing,
the airplane crossed over a fence near the runway
threshold, and the first pilot pitched the airplane
downward. The nose landing gear then contacted the
runway "hard," and the airplane began to bounce.
After two bounces, the first pilot increased power
on the left engine to "full," and pitched the airplane
up. He then told the second pilot that he was going
to abort the landing, and to reduce the flap setting
to 10 degrees. The airplane continued to pitch up,
yawed to the right, and "stalled" at an attitude
about 25 feet above ground level.
According to a written statement submitted by
the first pilot, following several previous flights,
the decision was made to demonstrate single engine
operations. He performed a practice single engine
approach, and missed approach, between 3,000 and
4,000 feet. The pilot then performed an actual single
engine approach to landing. During the entire approach,
nothing unusual was noted. During the touchdown,
"a slight bounce was encountered." The pilot judged
that the groundspeed was too fast in order to land
within the remaining runway, and elected to abort
the landing. He added full power and initiated a
climb, "at which time the aircraft slid off to the
right which resulted in a loss of directional control."
The owner/operator of the airplane witnessed
the accident, and described what he had seen during
a telephone interview.
He viewed the airplane as it was on the final
leg of the approach, and described that approach
as being "a little long, and a little fast." The
airplane then contacted the runway, and bounced
three times, with the nose landing gear contacting
the runway first, followed by the main landing gear.
The airplane s pitch angle then increased, and the
airplane "looked like it stalled." It then rolled
to the right, and the right wing contacted the ground.
Another individual witnessed the accident, and
provided a written statement. The witness was driving
on a highway adjacent to the airport, when he saw
the airplane "coming down very fast." The landing
gear contacted the ground, and the airplane bounced
back into the air, then turned right. As the airplane
was turning, it again began to descend, the right
wing contacted the ground, and separated from the
airplane. When asked, the witness stated that the
airplane initially touched down about 100 yards
from the runway end.
The wreckage was examined at the scene by Federal
Aviation Administration (FAA) inspectors, and no
anomalies were noted with the airframe, or either
engine.
The first pilot held an airline transport pilot
certificate with a rating for airplane multiengine
land, and a commercial pilot certificate with a
rating for airplane single engine land. His most
recent first class FAA medical certificate was issued
and at that time he reported 10,154 total hours
of flight experience.
The second pilot held an airline transport pilot
certificate with a rating for airplane multiengine
land, and a commercial pilot certificate with a
rating for airplane single engine land. His most
recent second class FAA medical certificate was
issued and on that date he reported 6,882 total
hours of flight experience.
The weather reported at Akron-Canton Regional
Airport (CAK), Akron, Ohio, included winds from
170 degrees at 6 knots, few clouds at 4,000 feet,
temperature 79 degrees Fahrenheit, dew point 62
degrees Fahrenheit, and an altimeter setting of
29.94 inches of mercury.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s improper flare and recovery from a bounced
landing, which resulted in a stall and subsequent
impact with the ground.
Source: National Transportation Board
Aircraft: De
Havilland DHC-2
Where: Anchorage,
AK
Injuries: None
Phase of flight: Landing
About 1705 Alaska daylight time, a float-equipped
de Havilland DHC-2 airplane received substantial
damage when it collided with trees and a private
residence following a loss of engine power while
on approach to land at the Lake Hood Seaplane Base,
Anchorage, Alaska. The solo commercial pilot was
not injured. The Title 14, CFR Part 91 personal
flight operated in visual meteorological conditions
without a flight plan. The flight departed a remote
lake near Beluga, Alaska, about 1635, and the destination
was the Lake Hood Seaplane Base.
The National Transportation Safety Board (NTSB)
investigator-in-charge (IIC) spoke with the pilot
of the accident airplane, and an Anchorage FAA Flight
Standards District Office inspector, at 1725. The
pilot spoke with the IIC from the accident site
using the FAA inspector s cellular phone. The pilot
related that he had departed a remote lake near
Beluga, and was on final approach to land at Lake
Hood, when the engine lost all power. The pilot
said it was a "fuel starvation event." He said he
had the fuel selector on the right fuel tank, and
thought the right tank was about 1/4 full, but the
engine stopped when he was about 300 yards from
the lake, and about 150 feet above the ground. He
reported that he had insufficient time or altitude
to switch to the belly tank and restore power, and
that he had to make an off-airport emergency landing.
The airplane subsequently struck trees, and then
a railing on the deck in the backyard of a private
residence on Lakeshore Drive, and came to rest in
the residence s garden, with the left wing resting
on the deck railing.
An FAA inspector at the accident site, and an
NTSB investigator who viewed the airplane the day
after the accident, noted structural damage to the
left wing.
In the NTSB Pilot/Operator Aircraft Accident/Incident
Report submitted by the pilot, he reported that
when he drained the fuel tanks prior to moving the
airplane, he recovered about one quart of fuel from
the right wing tank, and about 18 gallons from the
belly tank.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s incorrect positioning of the fuel tank
selector to a nearly empty tank, which resulted
in a loss of engine power due to fuel starvation,
and subsequent emergency landing at an off-airport
site.
Source: National Transportation Board
Aircraft:
Grumman American AA-1A
Where: Shreveport
LA
Injuries: 2 fatal
Phase of Flight: Takeoff
At 1346 central standard time, a Grumman American
AA-1A single-engine airplane was destroyed upon
impact with terrain following a lost of control
during initial takeoff climb near Shreveport, Louisiana.
The non-instrument rated private pilot and his passenger
were fatally injured. The airplane was owned and
operated by the pilot. Visual meteorological conditions
prevailed throughout the area for the 14 Code of
Federal Regulations Part 91 personal flight. No
flight plan was filed for the local flight that
originated as a flight of two airplanes, from the
Shreveport Downtown Airport (DTN) at 1342.
According to the air traffic control tower personnel
at the DTN airport, the airplane was cleared for
takeoff at 1342, as a flight of two airplanes, in
which a Cessna 120 airplane was the lead aircraft,
and the accident airplane was the trail airplane.
The pilot of the lead airplane maintained radio
contact with the trail airplane, and he observed
the trail airplane during his takeoff roll. Shortly
after takeoff, the pilot of the trail airplane reported
the he was in trail about a mile behind the lead
airplane. About 10 to 15 seconds later, the pilot
of the lead airplane reported that he looked back
to determined the location of the trail airplane.
He observed an airplane, which he did not immediately
recognize, entering a spin to the right; however,
he did not observe the airplane impact the terrain.
A few seconds later, the lead pilot reported
to the DTN tower that "[the Grumman] may have gone
down." Two additional airplanes circled the area
looking for the missing airplane. The wreckage was
located at 1427.
PERSONNEL INFORMATION
The pilot received his private pilot certificate
with an airplane single engine land rating in 1977.
According to the pilot s logbook, he accumulated
a total of 50.5 flight hours prior to discontinuing
his flying. In 2000, the pilot started flying
again in a Cessna 152 and in 2001 purchased the
accident airplane. According to his logbook, the
pilot had accumulated a total of 125.1 flight hours
as of his last entry on the logbook. The pilot was
estimated to have accumulated a total of 49.6 hours
in the accident airplane. The pilot completed his
most recent biennial flight review (BFR) in the
accident aircraft. He was issued an FAA Third Class
medical certificate, with a restriction to wearing
corrected lenses for near and intermediate vision.
AIRCRAFT INFORMATION
The 1971-model airplane was manufactured by Grumman
American Aircraft.. The most recent annual inspection
was completed at 823.2 aircraft hours (tachometer
time), approximately 16.22 hours prior to the accident.
The airplane was powered with a 4-cylinder Lycoming
O-235-C2C engine. The engine was driving a fixed
pitch, all metal, 2-bladed McCauley propeller, model
number SCM 71575, serial number G16035. A review
of the maintenance records revealed, the engine
accumulated a total of 2,894.72 hours, with 159.32
hours since its last engine overhaul.
According to data provided by several sources,
the airplane had been previously involved in a mishap
on July 20, 2001. The previous mishap was reported
to be the result of fuel starvation due to a defective
or improperly installed fuel selector valve, which
resulted in a forced landing near Monroe, Louisiana.
No records of the reported accident were available
in the NTSB or FAA accident database. As result
of the mishap, the airplane was reported to been
out of service until about 11 months later. All
necessary repairs were performed at a repair station
at the DTN airport.
COMMUNICATIONS
The pilot of the Cessna 120 aircraft reported
that he had been communicating with the accident
airplane on 123.45. No distress calls were received
from the pilot of the accident airplane on either
123.45 or on the tower frequency.
WRECKAGE AND IMPACT INFORMATION
The Global Positioning System (GPS) location
of the accident site, provided by a member of the
Sheriff Department, was recorded at 32 degrees 35
minutes and 35 seconds north latitude and 93 degrees,
45 minutes, 56 seconds west longitude.
The airplane impacted the ground in a 100-foot
wide pasture, which was oriented on a measured heading
of 340 and 160 degrees magnetic heading. The ground
was soft with several saturated sections. The nose
and main landing gear tires made ground impressions
varying in depth from 8 to 12 inches deep. The aircraft
impacted the ground and came to rest on a measured
heading of 280 degrees, approximately 4 nautical
miles from the departure end of the runway at DTN.
The engine remained partially attached to the
airframe. The two top engine mounts separated from
the airframe at the airframe mounting point as the
attaching hardware pulled out of the honeycomb.
The engine was found canted forward about 30 degrees
nose low. No evidence of a catastrophic engine failure
was noted. The barrel of the #3 cylinder showed
evidence of exposure to high heat (paint peeling
and bluing). Engine control continuity was established
to the throttle, mixture control and carburetor
heat. The mixture control was found in the full
rich position, the throttle was found in the closed
position, and the carburetor heat was found in the
cold/off position.
Five quarts of oil were present in the engine
crankcase. The oil had an olive-green color and
appeared to be clean. The propeller was rotated
by hand and continuity to the engine accessory section
was confirmed. The oil filter canister was removed
from the aircraft and opened for inspection during
the engine examination. No metal chips or any other
contaminants were found within the paper elements
of the oil filter.
The propeller remained attached to the engine.
The bottom half of the chromed spinner dome was
found crushed inwards and did not show any evidence
or signatures of rotational damage. No leading edge
damage was found on either propeller blade. One
propeller blade was found slightly bend aft about
5 to 10 degrees. The other blade was undamaged.
Approximately 2.5 ounces of straw colored fuel
were drained from the carburetor bowl during the
engine examination.
The muffler and some of the exhaust pipes were
crushed; however, the carburetor remained attached
to the engine, and appeared to be undamaged.
The windshield assembly was not compromised and
was found separated from the aircraft. The sliding
canopy, reported to have been removed by the first
responders, was found in the closed and locked position
at the time of the accident. The fuselage was buckled
in several areas. The underside of the airplane
was crushed upwards.
Both wings remained attached to the airframe.
There was no leading edge damage to either or the
wings or the horizontal stabilizers. The wings were
buckled and pushed upward. The flaps were found
extended to the 2/3 (two third) position. The elevator
trim indicator in the cockpit was found in the neutral
position; however, the elevator trim was found in
the full up (nose down) position.
All flight control surfaces, with the exception
of the rudder and vertical stabilizer, remained
attached to their respective surfaces. Flight control
continuity was established to the elevators, rudder,
and ailerons. The vertical stabilizer and the rudder
were found partially separated to the airframe,
and rotated towards the left side of the airframe.
The nose landing gear was folded in the aft direction.
The nose gear tire was destroyed by a minor post-impact
fire. The main landing gears were pushed up into
the skin for the lower portion of both wings. Also,
the gears were spread and the laminations of the
fiberglass main landing gear legs were spread. The
tubular nose landing gear assembly was buckled.
The fuel selector was found in the off position;
however, one of the first responders to the accident
later reported that the fuel selector had been found
in the left position and was moved to the off position
by one of the first responders. The aircraft s 12-gallons
tubular fuel cells were intact and not compromised.
Both fuel tanks were found near the full position.
Fuel was drained from both tanks during recovery.
The fuel drained from the airplane appeared to be
straw colored, and had the odor consistent with
automotive gasoline. No evidence of water contamination
was found in the gasoline.
The antennas on the bottom of the airplane were
crushed and found lying on their left side.
Neither of the two occupants of the airplane
made contact with the instrument panel during the
impact sequence, thus the instruments and gauges
were mostly undamaged. The airspeed indicator was
reading zero. The altimeter was reading minus 90
feet. The altimeter setting was found reading 30.14
inches. The directional gyro was reading 216 degrees.
The attitude indicator was level in a slight right
turn. The magnetic compass was reading 277 degrees.
The OBS on NAV 1 was set on 046 degrees. The clock
was stopped at 2:37. The Hobbs meter was reading
2,606.7 hours. The engine tachometer was reading
0839.32 hours. The fuel primer was found in the
locked position. The cabin heater was found in the
off position.
FIRE
The top of the battery case was found separated
from the fiberglass battery case. The inner side
of the battery case top had evidence of a post-impact
fire. The top of the battery did not show any evidence
of fire damage. Two of the screw-on filler caps
on the battery were missing.
The inside of the engine cowling showed evidence
of fire and smoke damage to the area above the engine
driven fuel pump. The electric fuel pump was wet
from an apparent leak. The fuel system was tested
for leaks on the airplane using the aircraft electrical
system. Fuel was observed leaking from the engine
driven fuel pump when the system was pressurized.
The inside of the side Plexiglas windows in the
airplane bore the smell of smoke; however, no evidence
of an in-flight fire was found in the engine compartment
or cabin. The airplane was not equipped with a hand-held
fire extinguisher.
METEOROLOGICAL INFORMATION
The 1353 METAR weather report from the DTN airport
reported winds from 310 degrees at 13 knots, gusting
to 22 knots, visibility 10 statute miles, with few
clouds at 4,100 feet, temperature 9 degrees Centigrade,
dew point of minus 1 degree Centigrade, and an altimeter
setting of 30.01 inches of Mercury.
MEDICAL AND PATHOLOGICAL
INFROMATION
An autopsy and toxicological tests were requested
and performed on the pilot. Forensic Pathologists,
Inc., of Bossier City, Louisiana, performed the
autopsy as requested by the Caddo Parish Coroner
s Office. The FAA s Civil Aero medial Institute
(CAMI) in Oklahoma City, Oklahoma performed toxicological
tests. Toxicological tests were negative for alcohol
or drugs.
SURVIVAL FACTORS
The airplane was found to be equipped with a
NARCO model ELT-10 electronic locator transmitter
(ELT). The ELT, which was installed in the tail
cone of the aircraft, was found to be in the "off"
position. The ELT battery was found to have expired
on the last annual inspection. The ELT did not operate
and thus did not aid in locating the wreckage of
the airplane.
The fire department was alerted as to the possibility
of an aircraft accident at 1359; however, the aircraft
was located from the air until 1427, approximately
41 minutes after the accident.
The airplane was equipped with shoulder harnesses
and seat belts for both occupant of the airplane.
The seat belts and shoulder harnesses had a "like-new"
appearance to them and it was assumed that they
had been installed at the time the interior was
refurbished. None of the seat belts or shoulder
harness was found stretched or damaged on any way.
According to the first responders, the passenger
was found in the cargo compartment located aft of
the two side-by-side seats.
Examination and evaluation of the signatures
of the damage sustained by seat tracks, the bottom
of both seat cushions, and both seat backs, were
consistent with both occupants of the airplane occupying
their respective seats at the time of the accident.
TEST AND RESEARCH
An engine examination and complete wreckage layout
examination was conducted. The engine was successfully
ran for 12 minutes. In order to facilitate the engine
run, the carburetor float assembly and the electrical
harnesses for both magnetos were replaced. Both
items had been fire damaged.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s failure to maintain adequate airspeed
resulting in a stall.
Source: National Transportation Board
Aircraft:
Grumman American AA-5B
Where: Barrett, TX
Injuries: 4 fatalities
Phase of Flight: Maneuvering
Approximately 1000 central daylight time, a Gulfstream
American AA-5B airplane was destroyed when it impacted
trees and terrain while maneuvering near Barrett,
Texas. The airplane was registered to and operated
by a Flying Club of Longview, Texas. The private
pilot and three passengers were fatally injured.
Visual meteorological conditions prevailed, and
a flight plan was not filed for the 14 Code of Federal
Regulations Part 91 personal flight. The cross-country
flight originated from Longview, Texas, at 0821,
and was destined for Galveston, Texas.
Witnesses, located at football fields near the
northwest end of the Texas Sport Ranch and the Rogers
private airstrip, reported that they observed the
airplane approach from the west, and it appeared
that it was going to land. As the airplane flew
by the witnesses, at about 30-60 feet AGL, the engine
"sounded like it was cutting out." After the airplane
passed by the witnesses, it pulled up and "suddenly
the engine cut out." The airplane turned left and
then nosed down into trees.
The Texas Sport Ranch and Rogers private airstrip
are located 36 nautical miles north-northwest of
the Galveston International Airport.
PERSONNEL INFORMATION
According to FAA records, the pilot was issued a
private pilot certificate with an airplane single-engine
land rating. The pilot was issued a third class
medical certificate. The medical certificate stipulated
limitations to use hearing amplification and wear
corrective lenses while operating an aircraft. According
to the last FAA medical application, the pilot reported
having accumulated a total of 120 flight hours,
of which 30 hours were in the previous six months.
The pilot s flight logbook was not located. According
to a representative of the flying club, within a
week of the accident, the pilot had accumulated
a total flight time of 127 hours, of which 56 hours
were in the accident airplane.
AIRCRAFT INFORMATION
The 1978-model Gulfstream American AA-5B, was a
low wing, single-engine, four-place airplane, which
had fixed tricycle landing gear. It was powered
by a Lycoming O-360-A4K engine rated at 180-horsepower,
and a McCauley, two-bladed, fixed pitch propeller.
Maintenance records were in the airplane at the
time of the accident and were destroyed by fire;
however, a few burnt pages, which were legible,
were recovered. The last recorded maintenance activity
on the engine was an oil change at a total aircraft
time of 4,054.4 hours and engine time since major
overhaul of 1,872.4 hours. At the time of the accident,
the airplane had accumulated a total time of 4,072
hours.
The representative of the flying club reported
to the NTSB investigator-in-charge (IIC) that the
aircraft had been flown on three cross-country trips
prior to the accident flight and no aircraft problems
were reported. The representative estimated that
the airplane departed on the day of the accident
with approximately 38 gallons of fuel.
METEOROLOGICAL INFORMATION:
At 0953, the William P. Hobby Airport (HOU), located
22 nautical miles southwest of the accident site,
reported the temperature as 86 degrees Fahrenheit,
and the dew point as 73 degrees Fahrenheit. According
to the carburetor icing probability chart, this
places the airplane in the serious icing range at
glide power.
WRECKAGE AND IMPACT INFORMATION
The accident site was located using a global positioning
satellite (GPS) receiver at 29 degrees 52.596 minutes
north latitude and 94 degrees 58.692 minutes west
longitude.
Examination of the accident site revealed that
the airplane impacted trees and continued through
the trees on a magnetic heading of 090 degrees for
90 feet before impacting the ground. The airplane
came to rest upright and partially on its right
side, on a magnetic heading of 081 degrees. The
airplane was consumed by fire. Both wings were separated
from the fuselage, and the right wing was found
lying near the left side of the fuselage. The entire
left wing spar was found next to the right side
of the main wreckage leaning up against a downed
tree. Flight control continuity was confirmed from
the cockpit to the left and right wing roots, the
rudder, and the elevator. The fuel selector was
found selecting the right fuel tank.
The engine remained attached to the mounts, but
separated from the firewall. Fire damage was noted
in all areas of the engine. The carburetor was separated
from its mounting flange, but remained attached
to the air-box remnants. The throttle plate was
found in the full open position, and the mixture
arm was in the full rich position. The fire damaged
carburetor was opened, and the float was found to
have incurred thermal damage. Both magnetos were
attached to their respective mounts and had incurred
fire damage. The magnetos did not spark when rotated
by hand. The vacuum pump also sustained fire damage.
The engine driven fuel pump body was burned away
from its mounting flange. The crankshaft rotated
freely and completely. Continuity was confirmed
to all rocker arms and the accessory gearbox. Thumb
compression was confirmed on all 4 cylinders.
The propeller remained attached to the crankshaft.
Both propeller blades exhibited minimal fire damage.
One propeller blade exhibited minimal impact damage.
The other blade exhibited some twisting with its
tip bent forward. The spinner remained attached
to the propeller, and it had a single crease near
its apex.
MEDICAL AND PATHOLOGICAL
INFORMATION
The Office of the Medical Examiner of Harris County
in Houston, Texas, performed an autopsy of the pilot.
There was no evidence found of any preexisting disease
that could have contributed to the accident.
Toxicological testing was performed by the FAA
Civil Aeromedical Institute s (CAMI) Forensic Toxicology
and Accident Research Center at Oklahoma City, Oklahoma.
The toxicological tests were negative for alcohol,
cyanide, and drugs. Carbon monoxide detected in
blood was 18 percent saturation.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s failure to maintain aircraft control
while maneuvering, which resulted in an inadvertent
stall. A contributing factor was the loss of engine
power for undetermined reasons.
Source: National Transportation Board
Aircraft:
Home built
Where: Peru, Indiana
Injuries: 1 fatal
Phase of Flight: landing
At about 1332 Central Daylight Time, an experimental
amateur-built Young Pietenpol Air Camper, piloted
by a recreational pilot, was destroyed on impact
with trees and terrain during a landing at Robison
Airport (IN33), near Peru, Indiana. The personal
flight was operating under 14 CFR Part 91. Visual
meteorological conditions prevailed at the time
of the accident. No flight plan was on file. The
pilot was fatally injured. The flight originated
from Logansport Municipal Airport, near Logansport,
Indiana, at time unknown and was landing at IN33
at the time of the accident.
The Miami County Sheriff s Department report
stated that the pilot s wife called two acquaintances
when the pilot did not return. The report said that
the acquaintances stated, "They were checking the
area from the air. ... They located the plane and
pilot. It appeared the pilot had been ejected and
it was noted his harness was broken."
The Sheriff stated that the pilot survived the
accident and was "transported to Parkview Hospital
via Samaritan helicopter."
The Miami County Sheriff s Department report
stated that the pilot died from his injuries about
0633.
The experimental amateur-built airplane was destroyed
on impact with trees and terrain during an attempted
landing. The recreational pilot reported on his
application for his last airmen s medical that he
had accumulated 70 total flight hours, 15 of which
were flown in the 6 months preceding that physical
examination. Local wind was 230 degrees at 11 knots.
The sheriff s report stated, "It appeared that possibly
the [airplane] struck the trees with [its] left
wing. There was fuel in the aircraft and it appeared
the engine was running at the time of the accident.
The [tachometer] was stuck at 1450 rpms." An on-scene
examination revealed no pre-impact anomalies. The
Final Forensic Toxicology Accident Report stated,
"DIPHENHYDRAMINE present in Urine." Diphenhydramine
(commonly known by the trade name Benadryl) is an
over-the-counter antihistamine with sedative effects,
most commonly used to treat allergy symptoms.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot not maintaining altitude/clearance from
the trees during the landing. A factor was the trees
he impacted.
Source: National Transportation Board
Aircraft:
Kitfox
Where: Spruce Pine,
GA
Injuries: 1 serious
Phase of Flight: Cruise
About 1030 eastern daylight time, a Kitfox experimental
homebuilt airplane, registered to and operated by
the pilot, was substantially damaged when it collided
with terrain following a loss of engine power during
cruise flight near Spruce Pine, Georgia. The private
pilot, the sole occupant aboard, received serious
injuries. Visual meteorological conditions prevailed,
and no flight plan was filed for the personal flight
being conducted under Title 14 CFR Part 91. The
flight originated from Avery County/Morrison Airport
in Spruce Pine, North Carolina, at 1015, with a
planned destination of Shiflet Airport in Marion,
Georgia.
According to the pilot, he was planning to fly
to Marion, Georgia, located 13.5 nm south of Spruce
Pine, Georgia, for the purpose of having an annual
maintenance inspection performed on the airplane.
The pilot stated that the taxi and run-up took approximately
five minutes, and he then departed on runway 16.
Shortly after departure, the pilot leveled off at
a cruising altitude of 1,000 feet above ground level.
Approximately 15 minutes after departure, while
three miles south of the departure airport, the
airplane s engine began to lose power. According
to the pilot, the engine "took about 45 seconds
to gradually quit." The airplane collided with trees
in a heavily wooded area, descended approximately
80 feet to the ground, then nosed over.
The pilot stated that five days prior to the
accident, he added five gallons of automotive fuel
to three existing gallons in the fuel tanks, and
departed with approximately 8 gallons of fuel in
the fuel tanks. The total fuel capacity is 12 gallons,
and the airplane burns approximately 3.9 gallons
per hour. At the time of the accident, the airplane
had flown 5 hours since the last inspection was
performed. An on-scene examination of the airframe
and engine by an FAA inspector revealed no mechanical
discrepancies. According to the inspector, evidence
of fuel was found at the accident site.
At 1020, weather conditions at Morgantown, North
Carolina, located 20 miles east of the accident
site, were reported as clear skies, a temperature
of 22 degrees C. (72 degrees F.) and a dew point
of 17 degrees C. (63 degrees C.). According to an
icing probability chart, weather conditions were
favorable for the formation of carburetor ice.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: A total loss of engine power due to
carburetor icing conditions. A factor was the mountainous,
unsuitable terrain on which to make a forced landing.
Source: National Transportation Board
Aircraft:
Lancair 235
Where: Tecumseh, MI
Injuries: None
Phase of Flight: Takeoff
A Miller Lancair 235, piloted by a private pilot,
sustained substantial damage when it departed controlled
flight and impacted terrain on takeoff from runway
18 (2,922 feet by 100 feet dry/turf) at the Tecumseh
Merillat Airport (34G), Tecumseh, Michigan. Visual
meteorological conditions prevailed at the time
of the accident. The personal, cross-country flight
was to be conducted on a visual flight rules flight
plan to Batavia, Ohio. The pilot reported no injuries.
In his written statement, the pilot said, With
mixture full rich and full throttle I started my
take off roll. After reaching 63 to 65 mph the aircraft
became air born with slight back pressure on the
stick. While trying to correct for cross wind from
about 190 [degrees] to 195 [degrees], I noticed
the aircraft was being blown to the right of the
runway in the direction of a row of trees and the
wind had shifted. At the same time, I noticed my
airspeed was becoming too low so I lowered the nose
of the aircraft to increase my airspeed. At this
point it appeared the aircraft was heading back
to the center of the runway when a gust of wind
caught the right wing and blew the aircraft just
enough for the left wing tip to touch the ground.
At this time I lost all control of the aircraft."
A Federal Aviation Administration inspector examined
the airplane at the accident site. The tail was
separated from the fuselage forward of the vertical
stabilizer. The outboard 2 feet of left wing to
the wing tip was split open. The nose gear was broken
aft and the propeller was splintered. An examination
of the airplane s systems revealed no anomalies.
Wind conditions recorded at Toledo Express Airport,
Toledo, Ohio, 24 miles south of the accident site,
were 210 degrees magnetic at 14 knots with gusts
to 20 knots.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s failure to maintain aircraft control
during the takeoff. Factors relating to the accident
were the crosswind and the wind gusts.
Source: National Transportation Board
Aircraft: Larson RV8
Where: Sequim, WA
Injuries: 2 fatal
Phase of flight: Maneuvering
An experimental amateur-built Larson RV8, N747CL, sustained substantial damage when it impacted terrain while maneuvering near the Sequim Valley Airport, Sequim, Washington. The airplane was registered to the pilot, and operated under the provisions of Title 14 Code of Federal Regulations Part 91. The two occupants, the airplane owner/front seat pilot, and the certified flight instructor (seated in the rear seat), were killed. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight. The local flight originated at Port Angeles, Washington, approximately 30 minutes before the accident. The pilot obtained a special visual flight rules (VFR) clearance for the departure at Port Angeles.
After departing Port Angeles, the pilot flew to Sequim Valley and completed a landing on runway 090. A witness reported that after the landing, the airplane departed to the west and entered a right downwind for runway 27. Witnesses reported that shortly after joining the downwind, the airplane began a steep, 60-90 degree, bank turn to the right. About 360 degrees into the turn, the airplane banked left, pitched nose-down and impacted terrain. The wreckage came to rest in a plowed field 1/4-mile north of the airport.
An inspector from the Federal Aviation Administration (FAA) Seattle Flight Standards District Office, reported that the purpose of the flight was to conduct a flight review for the airplane owner/front seat pilot.
The front seat pilot, age 68, held an airline transport pilot (ATP) certificate with ratings for airplane multi-engine land, and commercial privileges for airplane single engine land. The pilot possessed airline transport pilot type ratings for Boeing 747, McDonnell Douglas DC-10 and Lockheed 188 Electra airplanes. The pilot's total flight time was not obtained.
The rear seat pilot, age 61, held an airline transport pilot (ATP) certificate with ratings for airplane multi-engine land, and commercial privileges for airplane single engine land and airplane single engine sea. The pilot also held a certified flight instructor (CFI) certificate with airplane single engine land, multi-engine land and instrument airplane ratings.
The two-seat, low-wing, fixed-gear, Larson, RV-8 experimental amateur-built airplane received a special airworthiness certificate on February 18, 2008. The airplane was equipped with tandem seats and tandem flight controls. It was powered by a Superior XP-IO-360 series engine and equipped with a Hartzell propeller. The purpose of the flight was to complete a flight review for the owner of the airplane. According to witnesses near the accident site, the airplane had joined the right downwind leg of the traffic pattern for the runway when it subsequently began a steep 60- to 90-degree bank to the right. After completing about one full circle, the airplane banked back to the left, pitched nose-down, and impacted terrain. The wreckage came to rest in a plowed field 1/4 mile north of the airport.
Weather observations in the area during the time of the accident indicated wind from the northwest at 4 knots, visibility 10 miles and an overcast ceiling at 700 feet. Examination of the wreckage revealed extensive impact damage throughout the airframe. The forward section of the fuselage, cockpit area and associated instrumentation, were crushed aft to the main wing spar; the wreckage signatures and damage were consistent with a stall and/or spin. Examination of the airframe and engine revealed no evidence of a system malfunction or failure prior to the impact.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's failure to maintain adequate airspeed while maneuvering in the traffic pattern, which resulted in an aerodynamic stall.
Source: National Transportation Board
Aircraft:
Learjet 35A
Where: Marianna, FL
Injuries: 2 fatal
Phase of Flight: Landing
The pilot canceled the IFR flight plan as the
aircraft crossed the VOR and reported the airport
in site. The last radio contact with Air Traffic
Control was at 0935:16. The crew did not report
any problems before or during the accident flight.
The distance from the VOR to the airport was 4 nautical
miles. Witnesses saw the airplane enter right traffic
at a low altitude, for a landing on runway 36, then
turn right from base leg to final, less than 1/2-mile
from the approach end of the runway. Witnesses saw
the airplane pitch up nose high, and the right wing
drop. The airplane than struck trees west of the
runway, struck wires, caught fire, and impacted
on a hard surface road.
This was a training flight for the left seat
pilot to retake a Learjet type rating check ride
he had failed. He failed the check ride, because
while performing an ILS approach in which he was
given a simulated engine failure, and was transitioning
from instruments to VFR, he allowed the airspeed
to decrease to a point below Vref [landing approach
speed]. According to the company s training manual,
"...if a crewmember fails to meet any of the qualification
requirements because of a lack in flight proficiency,
the crewmember must be returned to training status.
After additional re-training, an instructor recommendation
is required for re-accomplishing the unsatisfactory
qualification requirements." The accident flight
was dispatched by the company as a training flight.
On the accident flight a company check airman was
in the right seat, and the check ride was set up.
The flight arrived an hour and a half late. The
accident flight was the first flight that the left
seat pilot was to receive retraining, and was the
only opportunity for him to demonstrate the phase
of flight that was unsuccessful during the check
flight. Examination of the airframe and engine did
not reveal any discrepancies.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s failure to maintain control of the airplane
while on final approach resulting in the airplane
striking trees. Factors in this accident were: improper
planning of the approach, and not obtaining the
proper alignment with the runway.
Source: National Transportation Board
Aircraft:
Luscombe8A
Where: Wahoo, NE
Injuries: None
Phase of Flight: Landing
Instruction
A Luscombe 8A nosed down while landing on runway
20 (4,101 feet by 75 feet, concrete) at the Wahoo
Municipal Airport, Wahoo, Nebraska. The certified
flight instructor (CFI) and the private pilot (student)
were not injured. The airplane received substantial
damage to the firewall. The instructional flight
was operating in visual meteorological conditions
without a flight plan. It originated from a private
airstrip in Lincoln, Nebraska.
The purpose of the flight was for the private
pilot/student to receive instruction for a tailwheel
endorsement. The student reported that they spent
about one hour practicing takeoffs and landings
on the grass runway with a 30-degree crosswind.
The CFI reported that the student was progressing
very well, so they decided to switch to the concrete
runway 20. The CFI reported the second landing on
runway 20, with a 60 degrees crosswind, was normal
and there was no tendency to ground loop.
The CFI reported that as the airplane slowed
during the landing roll, it nosed down despite "...elevator
efforts to stop it." He reported that either the
student had over braked or the brake system was
not functioning properly. The student reported that
"On second landing, during rollout, either I pushed
too much brake or we both pushed the same brake
and the aircraft nosed over."
The student pilot reported that at the time of
the accident, the local winds were from 140 degrees
at 10 knots.
Inspection of the airplane was conducted by an
inspector from the Federal Aviation Administration,
Lincoln, Nebraska, Flight Standards District Office.
The inspector reported the engine mounts were pushed
back into the firewall. He also reported that there
was no mechanical failure/malfunction of the brake
system, which would have resulted in the excessive
braking.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The student, who was a private pilot, used excessive
braking during the landing roll.
Source: National Transportation Board
Aircraft: Maule M-5-235C
Where: Kelton, UT
Injuries: None
Phase of flight: Landing
The private, non-instrument-rated pilot reported departing on a local personal flight. About 45 minutes after departure he encountered reduced visibility and elected to perform an off-field landing on a road. During the landing roll the airplane encountered a snow bank and nosed over. The airplane sustained substantial damage to the vertical stabilizer, rudder, and left wing during the accident sequence. The closest weather reporting station to the departure airport reported a visibility of 3/4 miles, mist with a few clouds at 400 feet above ground level, and a broken layer at 1,200 feet about the time of departure. The same station reported visibilities of 1/4 mile, fog, with a broken cloud layer of 200 feet, and overcast 700 feet at the time of the accident. The pilot did not obtain a weather briefing prior to departure; he additionally reported no preexisting mechanical malfunctions or failures with the airplane.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The non-instrument-rated pilot's decision to take off and fly into marginal weather conditions.
Source: National Transportation Board
Aircraft:
Mooney M20C
Where: Lakeland, FL
Injuries: 1 Serious,
1 Uninjured
Phase of Flight: Taxiing
A Mooney M20C collided with a ground marshaller
during taxi from landing at Lakeland Linder Regional
Airport, Lakeland, Florida, while on a personal
flight. Visual meteorological conditions prevailed
and no flight plan was filed. The airplane received
minor damage and the private-rated pilot was not
injured. The ground marshaller received serious
injury. The flight originated from Sarasota, Florida,
the same day, about 1545.
The pilot stated he landed on runway 9 left and
taxied west on taxiway "D". As he approached the
intersection of taxiway "D" and runway 5-23, he
encountered a ground marshaller waving two orange
wands. The ground marshaller was standing such that
the left wingtip would clear him by 18 inches. The
marshaller, who was facing east, began waving his
wands and back stepping to the west. As the marshaller
was positioned at the airplane s 10:30 position,
he, the marshaller, turned 180 degrees toward the
west and bent down from the waist. His back was
toward the wing and his face was down toward the
pavement. The marshaller continued walking toward
the west and turned his head to face another marshaller.
The pilot turned to face the direction the airplane
was taxing. He then heard a loud bang and the airplane
rotated to the left about 15 degrees. He immediately
countered with right rudder and turned left onto
runway 5-23 and stopped. He looked back and saw
the ground marshaller on the ground parallel to
runway 5-23, with his head facing the approach end
of runway 5.
The ground marshaller stated N2652W approached
the point he was working, runway 5-23 and taxiway
"D". The sign on the airplane indicated the pilot
was going to aircraft camping. He signaled him through
the intersection, straight ahead. He had eye contact
with the pilot and the pilot acknowledged his signal.
The ground marshaller stated he turned 110-130 degrees
to signal the motorcycle rider that the aircraft
was going to aircraft camping. At this point, he
was struck and became unconscious.
A witness stated the airplane was moving at a
normal taxi speed as it approached the intersection
of runway 5-23 and taxiway "D". The ground marshaller
made signal contact with the pilot and determined
the pilot s destination. The marshaller made a 90-degree
turn to tell the witness, who was on a motorcycle,
where to lead the airplane. The ground marshaller
s back was to the airplane s outboard left wing.
As the airplane continued taxiing, the left wing
struck the ground marshaller in the back, knocking
him forward. The left wing then struck the ground
marshaller in the back of the head, knocking him
to the ground.
Another witness stated the marshaller read the
sign on the windshield [of the airplane] to verify
the airplane s destination and then flagged the
airplane on by. She heard the pilot give the engine
excess throttle and then the airplane appeared to
veer to the left. The marshaller had already begun
to turn and walk away when the left wing of the
airplane hit him on his right side from the back.
He was sent tumbling across runway 5-23.
THE CAUSE
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The inadequate visual lookout of the pilot and the
ground marshaller resulting in the ground marshaller
being struck by the wing of the taxiing airplane
and receiving serious injury.
Source: National Transportation Board
Aircraft:
Mooney M20J
Where: Lake Placid,
FL
Injuries: 1 Minor
Phase of Flight: Takeoff
On January 17, 2002, about 0700 eastern standard
time, a Mooney M20J, registered to a private individual,
operating as a Title 14 CFR Part 91 personal flight,
crashed into an orange grove in the vicinity of
Lake Placid, Florida. Instrument meteorological
conditions prevailed and no flight plan was filed.
The aircraft was destroyed and the private-rated
pilot, the sole occupant, sustained minor injuries.
The flight was originating from a private airstrip
4 miles southwest of the city of Lake Placid at
the time of the accident.
The pilot stated by telephone from the emergency
room of the Florida Hospital of Lake Placid a short
time after the accident that he estimated his takeoff
and crash occurred at about 0630. As to the events
leading up to the crash, he stated, "All I remember
is the lights on the runway. Anything after that
I cannot recall." The completed NTSB form 6120.
1/2 was returned on February 1, 2001 and in the
section labeled, "Recommendation (How could this
accident have been prevented)", the pilot wrote,
"Triple check gas supply in tank selected." During
a subsequent telephone conversation on March 3,
2001, the pilot stated the time of the accident
would probably be closer to 0700. He stated although
the flight service station briefer recommended that
VFR flight not be attempted due to existing and
forecast ground fog, he could see stars overhead,
and decided to depart. He acknowledged that there
may have been patches of fog down the runway, although
he could see runway edge lights clearly. He stated
he observed 32 gallons of fuel in the left fuel
tank and 26 gallons in the right fuel tank on the
evening prior to his early morning departure. There
was no evidence of fuel leakage under the right
wing during his preflight walk around inspection
that morning. He did not remove the wing tank fuel
caps for a visual confirmation of fuel quantity
during the walk around. He stated he weighs 200
lbs., his golf bag and clubs weigh about 50 lbs.,
and the fuel in the left wing weighed about 188
lbs. Not knowing that the right tank was very nearly
empty, the imbalance may have contributed to the
left drift on takeoff and to the loss of directional
control once airborne. He still had no recollection
of the loss of engine power, or of the crash, itself.
A Highland County Sheriff s Department deputy,
the first official on the scene at 0750, stated
that the orange grove is adjacent to the left and
right edges of the runway, and that the runway lights
existed only along the right edge of the runway.
He stated the aircraft tire tracks in the grass
revealed a continuous left drift during his takeoff.
As to the weather conditions, he stated the fog
was like "pea soup". No witnesses to the accident
could be located, but numerous local personnel confirmed
that foggy conditions prevailed at about 0730.
According to St. Petersburg, Florida, Automated
Flight Service Station personnel, at 0450 a person
represented as the pilot of the accident airplane
received a telephone weather briefing for cross-country
flight legs originating from Winter Haven, Florida,
with an eventual destination of Sioux City, Iowa.
Because of a combination of existing and forecast
reduced visibility due to fog in the Winter Haven
area, the flight service briefer stated to the pilot
that VFR flight was not recommended.
According to an FAA inspector dispatched to the
crash site, the airport s single, turf runway is
oriented east/west, and the pilot was using runway
27 when the accident occurred. Tire tracks on the
3,000-foot runway revealed that the lift-off point
was half way down the runway and the aircraft tracked
a continuous left drift throughout the takeoff roll.
Examination of the wreckage path revealed more downward
than forward momentum. The propeller blades and
spinner revealed no bending or evidence of power
being developed at impact. The left wing fuel tank
was almost full, the right fuel tank was empty,
and the cockpit fuel selector was positioned to
the right wing fuel tank. The inspector and responding
fire rescue personnel could find evidence of very
little fuel spill. Subsequent examination of the
wreckage revealed the right fuel tank was compromised
in the crash sequence, however, there was no evidence
of fuel being contained in the right tank, precrash.
The engine s fuel injection distributor block was
examined and found dry.
On February 28, 2001, the NTSB and a Sebring,
Florida, based certified engine repair station mounted
the aircraft s engine, on an engine stand, and started
and operated it three separate occasions. The engine
started instantly and ran smoothly up to 2,500 rpm
for 10 minutes. The magneto check was conducted
and rpm drop was within POH limits. Oil pressure
was steady at 100 psi. Engine components rendered
inoperative due to the crash, and that had to be
substituted or omitted for the engine run included,
the propeller governor, the oil cooler, the engine
driven fuel pump, two replacement intake pipes,
the exhaust stacks, and the club propeller.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The failure of the pilot to perform a proper preflight
inspection and his improper fuel tank selection
for takeoff, resulting in a loss of engine power
on takeoff due to fuel starvation, and the pilot
s failure to maintain directional control of the
aircraft resulting in an uncontrollable descent
and collision with orange trees and terrain.
Source: National Transportation Board
Aircraft:
Mooney M-20J
Where: Fort Pierce,
Florida
Injuries: 1 Minor
Phase of Flight: Climbing
A Mooney M-20J, N511G, registered to and operated
by a private individual, as a Title 14 CFR part
91 personal flight, incurred a loss of engine power
while climbing to cruise altitude, and the pilot
made a forced landing in Fort Pierce Florida. Visual
meteorological conditions prevailed, and no flight
plan was filed. The private-rated pilot received
minor injuries, and the airplane incurred substantial
damage. The flight originated in Fort Pierce, Florida,
the same day, about 1230.
According to the pilot, about 8 to 10 minutes
after takeoff, while still climbing, at an altitude
of about 5,000 feet, the airplane lost engine power.
The pilot further stated that the gauges showed
about 1,000 rpm, and the manifold pressure remained
at 25 inches. He said he operated the throttle,
and observed instruments while attempting to regain
power, but he could not regain power or determine
the reason for the power loss. He said he turned
the airplane back towards Fort Pierce, Florida,
and as it glided towards the airport, he communicated
with the air traffic control tower controller, and
declared an emergency. As the airplane glided toward
the airport the pilot said he became less certain
that he would reach it, so he selected a clearing
in which to execute a forced landing. Upon reaching
900 feet, he abandoned the approach to the airport
and made an approach to a clearing. While on short
final to land in the clearing, the right wing of
the airplane impacted the top of a pine tree, which
changed the path. The airplane pan caked into the
ground and bounced into an area of numerous 4-foot
high sand piles, coming to rest upright on top of
one of the piles.
A post crash examination of the airplane and
engine was performed by a FAA licensed mechanic,
under the supervision of an FAA inspector. The examination
revealed that the magneto had detached from its
mounted position, and was hanging by the ignition
harness behind the engine. The magneto had not been
damage, and the magneto drive gear was laying in
the accessory housing along with one "hold-down"
plate. The retaining nuts, washers and lock washers
were not recovered. When tested, the magneto operated
on all eight distributor outputs, and the impulse
coupler and the distributor wiring were intact and
undamaged. There was engine continuity as well as
valve action and compression on all cylinders. Engine
oil was present, and there was evidence that some
oil had leaked at the back of the engine. No anomalies
were noted to exist with the induction or fuel systems.
The airplane and engine had last received an
annual inspection when an overhauled engine had
been installed. The airplane and engine had accumulated
10 hours since the annual inspection.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
Improper magneto installation by maintenance personnel,
which resulted in the magneto detaching from the
engine and subsequent loss of engine power.
Source: National Transportation Board
Aircraft:
Mooney M20S
Where: Port Huron,
MI
Injuries: None
Phase of flight: Landing
A Mooney M20S, operated by a private pilot, collided
with a snow bank while landing on runway 04 (5,103
feet by 100 feet.) The pilot was not injured and
the airplane was substantially damaged. The 14 CFR
Part 91 flight was operating in visual meteorological
conditions without a flight plan.
The pilot reported he flew a practice ILS approach
to runway 04. The approach was terminated in a go-around
followed by VFR traffic pattern and full stop landing
on runway 04. He reported the winds were out of
the northwest at 10 knots. He then departed on runway
04 and made a left hand traffic pattern for another
landing. The pilot reported, "Final approach required
minimal crab to correct for crosswind and then mild
slip to maintain the centerline." He reported that
just prior to touchdown while 2 feet above the runway
" a significant gust ballooned the aircraft 5-6
ft. above the runway where the aircraft stalled
and began to settle abruptly with a nose high attitude."
He reported he applied power to recover, but could
not gain enough airspeed. The airplane veered to
the right and the right main landing gear contacted
the snow on the side of the runway. According to
the pilot, the airplane spun around clockwise into
the snow where it came to rest.
The local weather observation, taken 5 minutes
prior to the accident, reported winds from 270 degrees
at 11 knots, gusting to 18 knots.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The pilot failed to maintain directional
control of the airplane and the runway selected
resulted in a tailwind condition. Factors associated
with the accident were the gusty crosswind and the
snow bank.
Source: National Transportation Board
Aircraft: Mooney M20S
Where: West Chicago,
IL
Injuries: 3 Uninjured
Phase of Flight: Landing
At 2130 central daylight time, a Mooney M20S,
piloted by a commercial pilot, sustained substantial
damage when it veered off the side of the runway
and collided with airport signs and markings after
a hard landing on runway 10 (4,751 feet by 75 feet,
asphalt), at Dupage Airport (DPA), West Chicago,
Illinois. The pilot and two passengers were uninjured.
Night visual meteorological conditions prevailed
at the time of the accident. The business flight
was operating under the provisions of 14 CFR Part
91 without a flight plan. The flight originated
from Eagle County Regional Airport (EGE), Eagle,
Colorado, at 1500 mountain daylight time.
The pilot stated, "The flare was too high, the
aircraft dropped to the runway and bounced." The
pilot noted the aircraft bounced twice, and on the
second bounce he attempted a go-around. The pilot
reported applying full throttle and raising "what
was thought to be one notch of flaps." The pilot
reported the aircraft swerved left and then was
"overcorrected right" and subsequently swerved off
the right side of the runway, striking fixed objects
with the wing. The pilot reported he reduced the
throttle to idle when the aircraft ran onto a taxiway.
The pilot indicated the nose gear collapsed when
the aircraft transitioned from the grass onto the
taxiway.
The on-sight investigation revealed that the
aircraft exited the left edge of runway 10 at taxiway
E-6. The aircraft s right wingtip was found at the
intersection of taxiway E-6 and runway 10. A runway
light was found damaged near the path of the left
landing gear. The wreckage pattern and markings,
including eight propeller strikes, continued to
the east of runway 20 right. The left main landing
gear was found separated from the rest of the aircraft.
The taxiway sign for taxiway C was damaged and found
next to the wreckage path. The aircraft came to
a stop at the intersection of taxiways C and G.
Inspection of the airplane revealed that the
flap handle was in the "up" position, and the flaps
were in the fully retracted position. The tail of
the aircraft showed scraping along its underside,
and the tailskid was damaged. The blades were broken
from the propeller hub, exhibited blade twist, and
were bent aft. The left main landing gear was broken
off, and the nose gear was collapsed.
The leading edge of the right wing was dented
about two-thirds of the way up the span from the
fuselage in a pattern consistent with striking an
airport sign.
The weather reporting facility located at DPA,
reported the winds at 2153 as 120 degrees at 4 knots.
The pilot reported no mechanical problems with
the aircraft or powerplant.
THE CAUSE
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s improper flare, and the pilot s failure
to maintain directional control. Contributing factors
were the pilot s improper flare and his inadequate
recovery from a bounced landing.
Source: National Transportation
Board
Aircraft: North American SNJ-6
Where: Santa Rosa Beach, FL
Injuries: 2 fatal
Phase of flight: Maneuvering
At 1236 central standard time, a North American SNJ-6 was destroyed when it impacted the Gulf of Mexico about 1 mile south of Topsail Hill Reserve State Park, Santa Rosa Beach, Florida. The certificated commercial pilot and the passenger were fatally injured. Visual meteorological conditions prevailed. The airplane, part of a five-airplane formation, was not operating on a flight plan.
According to the formation lead pilot, all of the pilots of the five-airplane formation met about 1130 for a formation briefing. The flight took off about 1200, and flew westbound, over water along the east-west beach for about 4 miles, with cross unders and echelons practiced. A breakup and rejoin was accomplished, and the formation proceeded eastbound. After later turning to the south, away from the beach, another breakup was accomplished with subsequent maneuvering resulting in an in-trail formation headed eastbound. The accident airplane was number 5 in trail.
In interviews, the pilots indicated that some were performing aileron rolls while in trail. None were performing additional acrobatics such as loops or barrel rolls from that low of an altitude, which the formation lead pilot indicated was about 500 feet above the water. A trail pilot reported that the separation between the airplanes was about 2,000 yards.
A video card containing a video clip of the accident was provided via local authorities. The video, which was taken from the beach, showed the last four of the five airplanes in trail over the water, initially heading eastbound. Each airplane was videoed separately.
The video began with the number 2 airplane in the middle of the screen, about 225 degrees through a left aileron roll. The airplane then exited the left side of the screen about 270 degrees through the roll (left wing straight up and right wing straight down.)
The number 3 airplane then came into view from the right side of the screen, at what appeared to be a lower altitude, and with the left wing 20 to 30 degrees down. The airplane remained in that approximate attitude and altitude until it exited the left side of the screen.
The number 4 airplane then came into view from the right side of the screen in an approximately 30-degrees nose-up attitude. About mid-screen it began a roll to the left. The airplane exited the left side of the screen, still about 30 degrees nose up, having rolled about 90 degrees. The camera then panned to the left to capture an additional part of the roll, until the airplane exited the left side of the screen again, but about 180 degrees through the roll (upside down at that point) with the nose still several degrees above the horizon.
The number 5 airplane, the accident airplane, then came into view from the right side of the screen, about 30-degrees nose up, and 30-degrees left wing down. It subsequently rolled to the left, and appeared to reach 90 degrees (left wing down, right wing up) before the camera panned left and momentarily lost it from the right side of the screen.
The airplane then flew back into view, about 135 degrees through the left roll, and continued to a 180-degree (completely upside down) position. At that point, the airplane’s nose was slightly low in relation to the horizon, dropping to about 10-degrees nose low. The camera then again panned to the left, and the airplane again disappeared from the right side of the screen.
The airplane subsequently reappeared on the screen about 225 degrees through the left roll, at an estimated 15-degrees nose low, and began a turn to the right while continuing the left roll recovery. As the airplane reached a southerly heading, away from the beach, it passed through about 315 degrees of the left roll (right wing 45-degrees down), and the roll suddenly reversed. The wings briefly went vertical (left wing up, right wing down), the nose dropped, and as the airplane continued rolling to the right, it appeared to go slightly inverted. It then descended into the water about 90-degrees nose low, with the top of the airplane facing the beach. The right wingtip was the first part of the airplane to strike the water, and as it did, the angle of the wings in relation to the horizon was about 45 degrees.
The pilot, age 60, held a commercial pilot certificate, with ratings for airplane single engine land, multi-engine land, single engine sea, multi-engine sea, and instrument airplane. The pilot's logbook was not recovered. On his latest FAA second class medical application, the pilot indicated 5,400 hours of total flight time.
One of the other formation pilots stated that he observed nothing abnormal with the pilot on the day of the accident, that the pilot was very "upbeat" about flying that day, and that the pilot had last flown the accident airplane on the day prior to the accident.
Weather, reported at Destin Airport, about 10 nautical miles west of the accident site, at 1253, included clear skies, visibility 10 statute miles, winds from 190 degrees true at 7 knots, temperature 14 degrees C, dew point -3 degrees C, and an altimeter setting of 30.24 inches Hg.
The wreckage was located in 60 feet of water in the vicinity of 30 degrees, 20.69 minutes north latitude, 86 degrees, 16.79 minutes west longitude.
The wreckage was recovered by divers in pieces, with the largest piece being the fuselage with the engine attached. The tail was only attached by control cables. The wing center section was also recovered; however, the outboard wing sections were not recovered due to low subsurface visibility.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's failure to maintain airspeed during a low altitude over water aerobatic maneuver, which resulted in an aggravated stall/spin. Contributing to the accident were the pilot's loss of situational awareness and his decision to perform aerobatics at a low altitude.
Source: National Transportation Board
Aircraft:
Pitts Special
Where: Meridian, CT
Injuries: None
Phase of Flight: Landing
A homebuilt Pitts Special S-1was substantially
damaged during a landing at Meridian Markham Municipal
Airport (MMK), Meridian, Connecticut. The certificated
private pilot was not injured, and visual meteorological
conditions prevailed at the time of the accident.
No flight plan had been filed for the flight, between
Danbury Municipal Airport (DXR), Danbury, Connecticut,
and Meridian. The personal flight was conducted
under 14 CFR Part 91.
According to the pilot, he landed the airplane
on Runway 18. Upon touchdown, the tailwheel-equipped
airplane appeared to be on the left side of the
runway, so the pilot applied right rudder. The airplane
then veered to the right, so the pilot applied left
rudder. The airplane continued to the right, so
the pilot applied, and then locked, the brakes.
The airplane flipped over its nose, and onto its
back.
The pilot estimated the airspeed of the airplane
to be at 30 miles per hour when the accident occurred.
Winds, recorded at the airport 24 minutes before
the accident, were calm.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The pilot s loss of control of the airplane
during the landing roll, due to his locking of the
brakes.
Source: National Transportation Board
Aircraft:
Rans S-6 Experimental
Where: Wyatte, MS
Injuries: 2 fatal
Phase of Flight: Low
flight
An experimental Rans S-6 airplane impacted with
trees 5 miles south of Wyatte, Mississippi. Visual
meteorological conditions prevailed at the time
and no flight plan was filed for the 14 CFR Part
91 personal flight. The aircraft was destroyed.
The private rated-pilot and one passenger were fatally
injured. The flight had originated about 21 minutes
earlier from a private airstrip, near Wyatte.
According to one witness, when he first heard
the airplane ...it sounded to be flying lower than
most planes in the area. When it came into his view
he first saw the airplane between trees at the back
of his house, and it appeared to him as though the
airplane was running about half throttle...not at
full rpm. As it came into a clearing he said, ...it
appeared to start to turn toward the house (west),
it was headed northeast. The airplane then straightened
up and the front end started to rise. Before it
went behind the trees again the witness saw what
appeared to him to be about a 10 to 15 degree [nose]
up angle. He lost sight of the airplane for about
5 seconds and he said he heard the engine stall.
When the airplane came back into his view he saw
it in a roll, the nose turned down, and there was
no engine sound. In addition, as the airplane started
down it made about a 50 to 75 spiral, disappeared
behind trees, and as it went out of his sight, he
heard the engine rev up.... high rpm. Within 3 to
5 seconds he heard it hit the ground. He said, ...the
plane did not seem to be having engine trouble,
missing or sputtering at any time, it did seem to
be flying low and slow.
The other witness said the airplane passed over
him between 20 and 25 feet...with the motor making
excessive noise, popping, misfire sound, and banked
toward the left. The airplane was flying away from
him and it was making a type of fluttering sound,
the engine seemed to choke down and stopped. He
then heard the sound of the airplane hitting the
trees, and then black smoke.
According to the FAA inspector s statement upon
his arrival on scene he found the airplane resting
nose down against a tree heading generally in a
northerly direction. He stated that most of the
airplane had burned, destroying the cockpit and
instrument panel. It appeared that the airplane
had impacted with the top of a 40-foot tree and
continued to the ground nose first. The right wing
was found 25 feet to the left of the aircraft, and
had completely separated from the airframe. The
right wing did not display any fire damage. Control
continuity was established to the elevator and left
wing aileron. The right wing had some fuel, and
a small portion was drained and checked for clarity.
The fuel exhibited a blue/green color of 100LL,
and was clear with no signs of contamination. The
engine had burned, but the case was still intact.
The oil tank had separated from the engine and was
empty of oil. The engine could not be rotated by
hand at the propeller. The two bladed carbon fiber
blades were found torn off, and the carbon fibers
were spread out and exposed. The engine was removed
from the crash site for further examination and
teardown. The right wing fuel tank was removed and
displayed no damage or holes. About 2 quarts of
100LL fuel were drained from the tank. The fuel
was clean and no contamination was found.
The engine was disassembled in the presences
of the FAA, at the facilities of South Mississippi
Light Aircraft, Lucedale, Mississippi, on November
16, 2001. The examination of the engine did not
reveal any discrepancies.
According to a note in the FAA inspector s statement,
about the time of the accident the temperature was
reported as 16 degrees C, and the dew point was
0 degrees C. The inspector s statement said, the
carburetor icing chart curve shows this to be a
condition for encountering serious icing at glide
power.
The airframe, engine, and pilot s personal logbooks
were not found. FAA records showed that the pilot
had a total of 380 flight hours, in all aircraft,
as of his last flight physical. There were no records
found to give any history about the airframe or
engine.
MEDICAL AND PATHOLOGICAL
INFORMATION
According to the autopsy report the cause of death
was ...airplane crash...acute traumatic injuries....
No findings, which could be considered causal to
the accident, were reported.
Toxicological tests were conducted at the Federal
Aviation Administration, Research Laboratory, Oklahoma
City, Oklahoma, and revealed, No ethanol or drugs
detected.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: Failure of the pilot to maintain airspeed,
which resulted in an inadvertent stall/spin, and
subsequent impact with trees, while at a low altitude.
Source: National Transportation
Safety Board
Aircraft: Robinson R-22
Where: Bountiful, UT
Injuries: 2 minor
Phase of Flight: Precautionary landing
At approximately 1130 Mountain Standard Time, a Robinson R-22 helicopter rolled over onto its side during an off-airport precautionary landing about 10 miles east of Bountiful, Utah. The commercial pilot and his passenger received minor injuries, and the aircraft, which is operated by Suncrest Aviation, of Spanish Fork, Utah, sustained substantial damage. The 14 CFR Part 91 personal pleasure flight, which departed Bountiful Skypark about 20 minutes prior to the accident, was being operated in visual meteorological conditions. No flight plan had been filed.
According to the pilot, he was taking his father-in-law on a local sight-seeing flight, and while looking around the local area he flew east up Holbrook Canyon. As he started up the canyon, he encountered a slight wind gust, but he decided to continue on up the canyon. Eventually he encountered gusting variable wind conditions and significant downdrafts. He therefore decided to turn around and fly back out of the canyon. As soon as he started to turn around, the helicopter encountered a strong downdraft, and it began to sink rapidly. As it began to sink, the main rotor rpm began to slow, so the pilot increased power and lowered the collective. Although the pilot was able to fly out of this downdraft, the aircraft entered another strong downdraft, and once again it sank toward the terrain with its main rotor rpm decreasing. In order to stop the descent, the pilot raised the collective, but the helicopter continued to sink and once again the main rotor rpm began to decay. By that time the helicopter was very close to the terrain, and because he felt he had no other choice, when the pilot spotted an open area he decided to land instead of trying to fly further in the presence of the strong downdrafts. Although the pilot was able to successfully touch down in the open area, soon after the skids came in contact with the rough steeply-sloped mountainous terrain, the helicopter rolled over onto its side.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's improper decision to fly up a mountain canyon at low level without knowledge of the wind conditions. Factors associated with the accident are gusty winds, downdrafts, and rough/uneven terrain.
Aircraft:
Robinson R-22
Where: Borger, TX
Injuries: 2 fatal
Phase of Flight: In
flight
A Robinson R-22 Beta helicopter struck an electrical
pole and impacted terrain during a dark night cross-country
flight. Both pilots received fatal injuries, and
the helicopter was destroyed. Visual meteorological
conditions prevailed at the time of departure from
Gruver, Texas. A flight plan was not filed for the
personal flight with a planned destination of a
private helipad near Amarillo, Texas, approximately
70 miles southwest of Gruver.
A witness, the daughter of the pilots, stated
that approximately 2145, the helicopter circled
over her residence, located 10 nautical miles south
of the Gruver Municipal Airport, and then flew south
toward Morse, Texas, along the planned route of
flight.
Another witness stated that approximately 2210
she observed a "low flying aircraft" descending
from the clouds near the south side of Borger. The
witness spotted a "light" through a clear patch
in the clouds. The "light" descended to just below
the clouds and continued to travel south along Highway
207 toward Panhandle. The "light" appeared to be
at a height "just above the radio tower," which
has an elevation of 285 feet agl.
Local authorities received notification approximately
midnight that the helicopter had not reached the
planned destination. Search and rescue procedures
were initiated; however, search efforts were hampered
by the dark night, low ceilings, and fog.
The next day the helicopter was located on a
ranch south of Borger, adjacent to an oil pump jack.
The terrain at the accident site consisted of rolling
hills and sparse vegetation.
PERSONNEL INFORMATION
The pilots daughter observed her parents enter the
helicopter and reported that her father positioned
himself in the left cockpit seat, and her mother
positioned herself in the right cockpit seat. The
helicopter was equipped with dual flight controls;
therefore, which pilot was serving as pilot-in-command
(PIC) at the time of the accident is unknown. For
the purpose of flight experience documentation only,
the left and right seat pilots are listed in this
report as first and second pilots, respectively.
The first pilot held a private pilot certificate
with an airplane single-engine land rating. He received
a rotorcraft helicopter rating on August 8, 2000.
According to the pilot s logbook, at the time of
the accident, he had accumulated 231 flight hours
in all aircraft, and 172 flight hours in the make
and model of the accident helicopter. The first
pilot had accumulated 10 hours of night flying time,
and had not logged any instrument flight training.
In addition, he had accumulated 7.6 hours of day
and 0.9 hours of night flight from Gruver to the
private helipad and/or the private helipad to Gruver.
The second pilot held a private pilot certificate
with a rotorcraft helicopter rating. According to
the pilot s logbook, at the time of the accident,
she had accumulated 143 flight hours in the make
and model of the accident helicopter. The second
pilot had accumulated 6 hours of night flying time,
and had not logged any instrument flight training.
In addition, she had accumulated 11.2 hours of day
and 2.0 hours of night flight from Gruver to the
private helipad and/or the private helipad to Gruver.
AIRCRAFT INFORMATION
The two-bladed, two-seat, black and white Robinson
helicopter was issued a standard airworthiness certificate
on June 22, 1990. The helicopter was powered by
a 160-horsepower Lycoming O-320-B2C engine (serial
number L-16212-39A). At the time of the most recent
annual inspection, the airframe and engine had accumulated
a total of 954.5 hours. At the time of the accident,
the helicopter had accumulated 975.6 hours.
The helicopter was not equipped for flight in
instrument meteorological conditions. In addition,
an emergency locator transmitter (ELT) was not installed
on the helicopter, nor was one required.
METEOROLOGICAL INFORMATION
According to McAlester Flight Service Station personnel,
at 1447, one of the two pilots requested a weather
briefing for a flight to E19 that was to depart
from a location near Amarillo at 1830. There were
no additional weather briefings requested by either
pilot of the accident aircraft.
The forecast was "sky clear occasional broken
cirrus east. Becoming ceiling overcast 1,000 feet.
Visibility 3 miles mist." There were no AIRMETs,
convective SIGMETs, or non-convective SIGMETs issued
by the Aviation Weather Center pertinent to the
planned route of flight, and there were no PIREPs
relevant to the accident area.
At 2053, the weather observation facility at
Guymon Municipal Airport Guymon, Oklahoma, located
27 miles north of E19, reported clear skies, visibility
8 statute miles, wind from 120 degrees at 6 knots,
temperature 30 degrees Fahrenheit, dew point 27
degrees Fahrenheit, and an altimeter setting of
30.01 inches of Mercury.
At 2153, GUY reported clear skies, visibility
8 statute miles, wind from 110 degrees at 3 knots,
temperature 28 degrees Fahrenheit, dew point 25
degrees Fahrenheit, and an altimeter setting of
30.04 inches of Mercury.
The weather observation facility at Borger-Hutchinson
County Airport (BGD), located 5 miles north of the
accident site, was malfunctioning at the time of
the observations that follow:
- At 2151, BGD reported visibility 8 statute
miles, wind from 010 degrees at 10 knots, temperature
30 degrees Fahrenheit, dew point 27 degrees
Fahrenheit, and an altimeter setting of 30.00
inches of Mercury.
- At 2331, BGD reported broken clouds at 800
feet, visibility 8 statute miles, wind calm,
temperature 28 degrees Fahrenheit, dew point
27 degrees Fahrenheit, and an altimeter setting
of 30.04 inches of Mercury.
- At 2117, the weather observation facility
at Amarillo International Airport (AMA), located
28 miles southwest of the accident site, reported
broken clouds at 500 feet, visibility 9 statute
miles, wind from 120 degrees at 9 knots, temperature
36 degrees Fahrenheit, dew point 32 degrees
Fahrenheit, and an altimeter setting of 29.98
inches of Mercury.
- At 2153, AMA reported broken clouds at 300
feet, visibility 7 statute miles, wind from
100 degrees at 9 knots, temperature 30 degrees
Fahrenheit, dew point 30 degrees Fahrenheit,
and an altimeter setting of 29.96 inches of
Mercury.
- At 2253, AMA reported overcast ceiling at
300 feet, visibility 5 statute miles, wind from
110 degrees at 11 knots, temperature 30 degrees
Fahrenheit, dew point 30 degrees Fahrenheit,
and an altimeter setting of 30.01 inches of
Mercury.
- At 2330, the Texas/Oklahoma Panhandles Forecast
Discussion, issued by the National Weather Service
of Amarillo, Texas, reported "low clouds and
fog developing on the cool side of surface boundary...
from Amarillo to Dalhart. Surface dew point
spreads are low elsewhere...so have mentioned
low clouds and fog eastern and north-central
sections as well. Also mentioned light freezing
drizzle developing over south-central...southwestern...and
northwestern zones where advection of higher
dew points in easterly low-level flow will provide
environment favorable for development of same."
WRECKAGE AND IMPACT INFORMATION
The accident site was located on the 6666 Ranch,
0.9 miles east of Highway 207, approximately 37
miles south of E19, and 5 miles south of the radio
tower referenced by the aforementioned witness.
The helicopter wreckage was distributed along a
measured 250-foot path. The initial impact point
was a 30-foot tall electrical pole with an 8-foot
crossbeam.
The main wreckage consisted of the tail boom
with tail rotor attached, main rotor assembly, transmission,
engine, and the fuselage. Between the initial impact
point and the main wreckage, were numerous helicopter
components, including fragmented landing skids,
doors, flight instruments, and the cockpit instrument
console.
The engine and main transmission remained attached
to the airframe. The firewalls were buckled and
compressed. The engine was intact, and the carburetor
and exhaust pipes were crushed. The main rotor clutch
was found engaged. The clutch turned freely and
locked normally when turned by hand. The V-belts
were found off the upper and lower sheave grooves,
but the V-belts were visually intact.
The main rotor assembly, with its corresponding
remaining main rotor blades, was found adjacent
to the fuselage. The main rotor mast was separated
at the main transmission. The tail boom was separated
aft of the main fuselage. Tail rotor drive shaft
continuity was confirmed from the tail boom separation
point to the transmission, and also from the separation
point to the tail rotor gearbox. The damper was
found intact, and the shaft rotated freely within
the damper bearing. The aft flex coupling was intact.
The tail rotor system remained attached to the gearbox
and rotated freely by hand. The tail rotor blades
were found separated at the grips.
The main fuel tank was found connected to the
airframe, and the auxiliary fuel tank was found
separated from the airframe. The integrity of both
fuel tanks was compromised. The fuel caps on both
tanks were found secured.
An inspection and disassembly of the engine and
related components did not reveal any discrepancies
that would have precluded normal operation prior
to impact.
SEARCH AND RESCUE
According to a search and rescue mission report
by the Texas Wing Civil Air Patrol (CAP), CAP searches
were initiated February 17 through the 20th, 2001.
During the 179.6 hours of searching, there were
118 aerial and ground sorties conducted with 13
to 17 aircraft and 37 to 56 individuals searching
each day. The searched area extended outward from
Borger to the Oklahoma State Line on the north,
Pampa, Texas on the east, Panhandle on the south,
and Lake Meredith, Texas, on the west.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: the pilot s inadvertent flight into
instrument meteorological conditions and failure
to maintain obstacle clearance. Contributing factors
were the pilot s failure to obtain an updated preflight
weather briefing and the dark night conditions.
Source: National Transportation Board
Aircraft:
Socata TB-20
Where: Frederick,
MD
Injuries: 2 minor
Phase of Flight: Takeoff
At 1053 eastern standard time a Socata TB-20
was substantially damaged during a forced landing
following a total loss of engine power, after departing
from the Frederick Municipal Airport (FDK), Frederick,
Maryland. The certificated private pilot and passenger
received minor injuries. Visual meteorological conditions
prevailed and no flight plan was filed for the local
personal flight conducted under 14 CFR Part 91.
The pilot stated that he performed a complete
preflight inspection and noticed no abnormalities
with the engine. During the initial takeoff climb
from runway 30, at an altitude of 400 feet, he noticed
the engine power decrease to 1,500 rpm, and several
seconds later, the engine lost complete power. The
pilot then performed a forced landing to a soft
field, during which the wings and fuselage of the
airplane were substantially damaged.
A Federal Aviation Administration (FAA) inspector
performed a preliminary examination of the airplane
after the accident. According to the inspector,
he observed about 2-3 gallons of fuel in the left
wing fuel tank; however, the tank was breached.
The inspector reported there was "sufficient" fuel
in the right tank. Examination of the cockpit throttle
and propeller controls revealed they were in the
full forward position, and the mixture control,
which sustained impact damage, was in the 3/4 full
forward position. The spark plugs were removed,
and no anomalies were noted. The fuel servo displayed
impact damage, and the fuel inlet line was separated
from the inlet side of the servo.
The engine was test run on the airframe with
a replacement fuel injector and fuel line. The engine
started, and ran for several seconds, without any
anomalies, before being shut down.
The National Transportation Safety Board s Metallurgical
Lab examined pictures taken of the fuel injector
inlet line, by an electron scanning microscope.
According to the Metallurgical Lab, the damage to
the fuel line was consistent with impact damage,
and no evidence of cross-threading was noted.
According to the operator of the airplane, it
had been topped off with fuel the day prior to the
accident, and had flown about 2.5 hours since then.
A 100-hour inspection had been performed on the
airplane and the airplane had flown approximately
8 hours since then.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
Total loss of engine power for undetermined reasons.
Source: National Transportation Board
Aircraft: Swearingen SA-226-TC
Where: Denver, CO
Injuries: None
Phase of Flight: Takeoff
A Swearingen twin-engine turboprop airplane operated as Key Lime 515, sustained an in-flight failure of an elevator control cable during initial climb from the Denver International Airport, Denver, Colorado. The airplane was registered to EDB Air, Inc., Wilsonville, Oregon, and operated by Key Lime Air, Inc., Englewood, Colorado. Visual meteorological conditions prevailed at the time of the incident. The unscheduled domestic cargo flight was being operated under the provisions of Title 14 Code of Federal Regulations Part 135 under an instrument flight rules flight plan. The airline transport pilot, who was the sole occupant, was not injured. The flight was originating at the time of the incident and was en route to Dodge City, Kansas.
According to a statement provided by the pilot, prior to departure he completed the pre-takeoff checklist, which included checking the flight controls. While at 80-85 knots during the takeoff roll, the pilot "noticed pitch seemed very light. At rotation speed, the pilot pulled back on yoke and aircraft left ground. At this point, the yoke came all the way back and aircraft began to quickly pitch upward." The pilot reported that moving the yoke forward had no effect and it felt disconnected from the elevators. The pilot quickly began to trim nose down and reduced power to stop excessive nose up pitch. After gaining marginal control of the aircraft, the pilot advised air traffic control he had a "flight control problem" and requested a return for landing.
During the downwind leg to runway 17L, the pilot "experimented with various configurations...to determine the method of approach and landing." The pilot executed a gradual descent to the runway and landed uneventfully.
Examination of the airplane by company maintenance personnel revealed that "the elevator down cable was improperly routed at the pulley in the vertical stab, just below the elevator bell crank. This caused the cable to wear against a guide until the cable failed." Upon discovery of the improper routed cable, the operator checked the other 18 aircraft in their fleet. No discrepancies were found.
According to the aircraft maintenance records, the elevator cable was installed by another operator, as required by Airworthiness Directive 87-02-02. Key Lime Air, Inc. maintained the aircraft under a manufacturer approved continuous airworthiness inspection program. The aircraft underwent a "Letter Check E" inspection. According to the inspection checklist, the elevator cables and related components were inspected with no anomalies noted.
The National Transportation Safety Board determines the probable cause(s) of this incident to be: the failure of the elevator down cable due to an improperly routed cable by unknown maintenance personnel. A contributing factor was the improper inspection of the elevator cable by the operator's maintenance personnel.
Aircraft:
Swearingen SA-227-AT
Where: Fayetteville,
AR
Injuries: None
Phase of flight: Landing
A Swearingen SA-227-AT twin-engine airplane was
substantially damaged during a wheels up landing
at the Fayetteville Airport, Fayetteville, Arkansas.
The airline transport pilot, acting as the captain,
and the commercial pilot, acting as the first officer,
were not injured. Night visual meteorological conditions
prevailed and an instrument flight rules flight
plan was filed for the Part 135 air taxi cargo flight.
The flight originated from Tulsa, Oklahoma, and
was terminating at the time of the accident.
According to the 4,116-hour captain, the crew
experienced a problem with the crew intercom system
during departure, and the first officer (flying
pilot) had to "repeat his requests three or four
times" before the captain could hear him. The crew
decided they would notify the maintenance personnel
when they arrived at their destination.
The captain reported that air traffic control
issued a clearance to descend to 3,000 feet "at
pilot s discretion." The crew initiated their descent
at a later than normal distance from the airport.
The first officer needed to reduce the power below
25 percent torque in order to expedite the descent,
which set off the gear warning horn. The sound eventually
became part of the background noise.
The captain added that at 2 miles from the final
approach fix (FAF), he asked the tower to dim the
runway lights. At that time, the runway and approach
lights went out and the crew lost sight of the runway.
While the captain was asking the tower to turn the
lights back on, the first officer called gear down,
syncs off, speeds high, below the line check list.
The captain did not hear the first officer s callout
and did not lower the landing gear. The captain
stated that he did not hear the first officer s
callout either because of the conversation [he]
was having with the tower or because of the intercom
difficulties.
As the approach continued, the first officer
had a problem slowing the airplane to proper approach
speed. The airplane touched down on the runway with
the landing gear retracted, slid approximately 2,500
feet and exited the left side of the runway. According
to the FAA inspector, who examined the airplane,
two pressure bulkheads were structurally damaged.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The flight crew s failure to extend
the landing gear. Contributing factors were the
flight crew s non-compliance with the checklist,
the pilot-in-command s diverted attention as a result
of the loss of instrument approach/runway lighting,
the partial failure of the instrument approach/runway
lighting system, and the partial failure of the
intercom system.
Source: National Transportation Board
Aircraft: Schweizer 269C
Where: Santa Rosa, NM
Injuries: None
Phase of flight: Landing
According to the written statement provided by the flight instructor, during the cross country flight they elected to divert due to thunderstorms building in the area. While on approach to runway 19, the helicopter encountered a wind gust (estimated to be 45 knots) and "lost tail rotor authority." The flight instructor immediately took control of the helicopter, from the student; however, the tail rotor struck the runway. The flight instructor was able to level and land the helicopter without further incident. The helicopter was examined by a Federal Aviation Administration inspector revealing that one frame tube was broken, the skid cross tube was bent, and a tail rotor blade was damaged. The flight instructor confirmed that there were no mechanical anomalies with the helicopter prior to the accident.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The student pilot's failure to maintain control of the helicopter while landing in gusty surface winds conditions. Contributing to the accident was the flight instructor's inadequate monitoring of the flight.
Aircraft: Taylorcraft BC12-D
Where: Gold Hill, NC
Injuries: 1 serious
Phase of flight: Landing
According to the pilot, on the first landing attempt he was going to do a three point landing. On touchdown the airplane "darted" to the left. He then came back across the runway going toward the right side, but got it airborne before it could go off the runway. He climbed out and continued in the pattern for another landing. He said he wanted to get the airplane on the ground to try and find out why it darted to the left. His second landing attempt was going to be another three point landing. On touchdown the airplane darted to the right. The airplane was angled toward a two story house. He then pulled the control wheel aft to keep it on the ground and "ride it out." He said that was a mistake because the airplane then bounced. He pushed the nose over and he thinks he had some power on. When he saw that he would hit the house if he continued, he added full power and pulled back to climb. The airplane then stalled and the right wing dropped and he crashed. Examination of the airplane by an FAA Inspector found no mechanical problems with the aircraft structure, flight controls, or engine. A review of the pilot's log book found that the pilot total flight time in all aircraft was 346 hours. The pilot received his tail wheel endorsement August 2, 1998, and had accumulated a total of 48 hours since that endorsement. At the time of the accident, the pilot had logged 3.5 hours of total flight time since January of 2006.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's failure to maintain airspeed while doing a go around, which resulted in an inadvertent stall, loss of control and in-flight collision with the ground. A factor was the pilot's lack of recent experience in the airplane.
Source: National Transportation Board
Aircraft:
Teratorn
Where: Elbow Lake. Minnesota
Injuries: 1 fatal
Phase of Flight: Cruise
About 0630 Central Daylight Time, an unregistered
Teratorn two-place airplane, piloted by a private
pilot, was destroyed on impact with terrain about
three quarters of a mile west of the Elbow Lake
Municipal Airport (Y63), near Elbow Lake, Minnesota.
The personal flight was operating under 14 CFR Part
91. Instrument meteorological conditions prevailed
at the time of the accident. No flight plan was
on file. The pilot was fatally injured. The flight
originated from a private airstrip near Elbow Lake,
Minnesota, about 0600, and was en route to Y63 at
the time of the accident.
The Grant County Sheriff s report stated that
prior to the flight the pilot s wife told the accident
pilot that the weather conditions at Elbow Lake
Airport were foggy. The report said that the accident
pilot replied that he could see the tops of the
trees "and he was going to fly low and follow the
rail road tracks into Elbow Lake."
The Grant County Sheriff s report stated:
[The accident pilot s brother] told me that he had
flown from Fergus Falls to Elbow Lake this morning
looking for his brother s plane which had not arrived
at the Elbow Lake Airport. ... [He] then called
[his brother s wife] and ... asked what direction
[the accident pilot] was taking to get to the airport.
[She] said that he was following the train tracks
east that come from Wendell to Elbow Lake. [He]
then flew over the railroad tracks and followed
them east to Elbow Lake and found his brother s
plane in the wheat field. ... [He] said that it
was too foggy to be flying. The only reason he was
flying was to look for his brother.
PERSONNEL INFORMATION
The pilot held a private pilot certificate with
a single-engine land airplane rating. His FAA third-class
medical certificate was issued with a limitation
for corrective lenses. On his application for that
flight physical, the pilot reported that he had
accumulated 12 total flight hours. On his application
for that certificate, the pilot reported that he
had accumulated 45.8 total flight hours of which
3 hours were listed as instrument flight time.
AIRCRAFT INFORMATION
The accident airplane was an unregistered Teratorn,
two-place airplane. The original kit manufacturer
is no longer in business. The airplane s original
kit builder could not be confirmed. The accident
airplane was a single-engine, high-wing airplane.
Its engine was a 64-horsepower Rotax 532 engine,
serial number 3488536. The engine was shipped from
its manufacturer in April of 1985 to Teratorn Aircraft.
The propeller was a three-bladed, 66-inch diameter,
Warp Drive propeller. The propeller was shipped
from its manufacturer on July 31, 1994.
METEOROLOGICAL INFORMATION
At 0555, the Fergus Falls Municipal Airport-Einar
Mickelson Field (FFM), near Fergus Falls, Minnesota,
about 15 miles and 330 degrees from the accident
site, recorded weather was: Wind 340 degrees at
7 knots; visibility 1 1/4 statute miles; present
weather mist; sky condition overcast 200 feet; temperature
16 degrees C; dew point 15 degrees C; altimeter
29.94 inches of mercury.
At 0615, the FFM recorded weather was: Wind 330
degrees at 7 knots; visibility 3/4 of a statute
mile; present weather mist; sky condition overcast
200 feet; temperature 16 degrees C; dew point 15
degrees C; altimeter 29.94 inches of mercury.
At 0635, the FFM recorded weather was: Wind 350
degrees at 7 knots; visibility 1/4 of a statute
mile; present weather fog; sky condition overcast
200 feet; temperature 16 degrees C; dew point 15
degrees C; altimeter 29.94 inches of mercury.
At 0655, the FFM recorded weather was: Wind 350
degrees at 7 knots; visibility 3/4 of a statute
mile; present weather mist; sky condition overcast
200 feet; temperature 16 degrees C; dew point 15
degrees C; altimeter 29.95 inches of mercury.
WRECKAGE AND IMPACT INFORMATION
The Grant County Sheriff s report stated: The
nose of the aircraft was pushed back to the left
side and the plastic door was in front of the aircraft
about 15 feet. The motor appeared to have pushed
forward and snapped off two of three propellers.
The wings also had damage to the front of them.
...
There was a considerable amount of damage to
the cockpit area of the aircraft and it appeared
that the aircraft had nose dived directly into the
ground, bounced back up into the air, and landed
upright, approximately 10 yards away from an area
where you could see the plane possibly hit.
MEDICAL AND PATHOLOGICAL
INFORMATION
An autopsy was performed at the Department of
Pathology, Lake Region Healthcare Corporation, in
Fergus Falls, Minnesota.
The FAA Civil Aeromedical Institute prepared
a Final Forensic Toxicology Accident Report. The
report was negative for the tests performed.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot s intentional flight into known fog and
failure to maintain aircraft control during cruise
flight. A factor was the fog, and the low altitude
flight.
Source: National Transportation Board
Aircraft:
Thorp Amateur-Built
Where: Imperial, TX
Injuries: 2 fatal
Phase of flight: Cruise
At 1400 central daylight time, a Holt Thorpe
T-18C amateur-built experimental airplane was destroyed
when it impacted terrain following an in-flight
separation of a propeller blade near Imperial, Texas.
The private pilot, who was the registered owner
of the airplane, and his passenger, sustained fatal
injuries. Visual meteorological conditions prevailed
and a flight plan was not filed for the personal
flight. The local flight originated from the Roy
Hurd Memorial Airport, Monahans, Texas, approximately
1345.
According to witnesses, the airplane was in cruise
flight southwest bound, between 1,500 and 2,500
feet agl, when they heard a loud noise and observed
pieces of the airplane separate from the airframe.
Subsequently, the airplane entered a descent and
impacted the ground. A fire erupted and consumed
the airplane.
The FAA inspector, who examined the airplane,
reported that the airplane was equipped with a Lycoming
IO-360-B1E engine and a Hartzell HC-F2YR-1F, 2-bladed,
constant speed propeller. Sections of the engine
cowling were located approximately 1 mile northeast
of the accident site. Further examination revealed
that one of the two propeller blades had fractured
and a portion was missing. The missing portion of
the blade was not recovered. The propeller was disassembled
and the fractured blade was sent to the NTSB Materials
Laboratory in Washington, D.C for further examination.
The NTSB metallurgist reported that the blade
fractured 14.5 inches from the butt end. The fracture
surface appeared relatively flat and parallel to
the chordwise plane with a smooth, curving boundary,
typical of fatigue. The fatigue features emanated
from an intergranular fracture area that was covered
by a corrosion product. The metallurgist added that
the blade length was not consistent with the original
manufacturing specifications. On-scene measurements
revealed that the total length of the blade was
32 inches, corresponding to a propeller diameter
of 66 inches. When manufactured, the propeller diameter
was 80 inches.
According to the propeller manufacturer, the
recommended time between overhaul on the accident
propeller is 2,000 hours or 5 years, whichever comes
first. According to the airplane s maintenance logbooks,
the propeller had accumulated a total of 369 hours
at the time of its last overhaul. When the airplane
underwent its most recent condition inspection,
the propeller had accumulated a total of 743 hours.
There was no record of the propeller undergoing
an overhaul since 1991. Additionally, the HC-F2YR-1F
propeller was not approved by the manufacturer for
installation on the Lycoming IO-360-B1E engine.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The failure of the propeller blade due
to fatigue, which originated from a corrosion crack.
A contributory factor was the pilot/owner s failure
to ensure that the propeller was overhauled at the
manufacturer s recommended interval.
Source: National Transportation Board
Aircraft:
Vari-Eze
Where: Iowa City,
IA
Injuries: 1 minor
Phase of Flight: Forced
landing
An experimental-amateur built Fowler Vari-Eze
sustained substantial damage when it nosed-over
during a forced landing following a loss of engine
power while in cruise climb. Visual metrological
conditions prevailed at the time of the accident.
The personal flight was not on a flight plan. The
pilot, the sole occupant, reported minor injuries.
The flight departed the Iowa City Municipal Airport,
Iowa City, Iowa, at 0817, for the local test flight.
According to the pilot s written statement, the
purpose of the flight was to evaluate engine cooling
performance subsequent to the engine being overhauled
and a modification to the engine exhaust system.
The pilot reported, I climbed to pattern altitude,
800 AGL [above ground level] and leveled off to
observe the engine temperature. I observed engine
temperatures in the normal range, very efficient
cooling, so I turned away from the airport. I retracted
the nose wheel and advanced throttle to climb above
pattern altitude. At this point the engine faltered
and stopped. There was no windmilling of the propeller,
because the propeller is a short-bladed pusher type
mounted in the aft section of the fuselage.
The pilot stated, Because of the low altitude
at which the engine ceased operating, I was unable
to consider any attempt to make the airport [Iowa
City Municipal Airport] and immediately selected
the best available field. The only field long enough
contained standing corn about 7 in height. The aircraft
was damaged while landing in the corn.
The pilot stated, After the engine stopped there
was not sufficient time to diagnose the problem,
switch tanks and re-start the engine. I felt it
was best to give priority to controlling the aircraft,
selecting the best field available and preparing
and performing the best possible forced landing
under the circumstances.
The pilot reported, I discovered subsequently
that a fuel-drain petcock had been installed that
was of a different type than that which had been
in the aircraft previously. It was not appropriate
for the location in the aircraft because the petcock
position in the Vari-Eze is well up under the cowling
and is difficult to observe visually. Draining the
fuel sump must be done primarily by feel. The petcock
had stuck partially open. I believe that the header
tank was drained through the partially open petcock
during the first few minutes of flight.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows. The inadequate preflight by the pilot
which resulted in the fuel drain remaining partially
open. Factors to the accident were the loss of engine
power due to fuel starvation, the partially open
fuel drain, the unsuitable terrain for landing encountered
by the pilot during the forced landing, and the
corn crop.
Source: National Transportation Board
Aircraft: Homebuilt
Where: Rush City,
MN
Injuries: 1 fatal
Phase of Flight: Maneuvering
An amateur built, experimental Wolter Avid Flyer
sustained substantial damage when it stalled at
about 150 feet agl and impacted the terrain. The
pilot received fatal injuries.
A witness, who was a certified flight instructor
and operated a flight school, reported the pilot
had been practicing taxiing the airplane on a 4,400
foot, asphalt runway at Rush City Regional Airport
(ROS) at Rush City, Minnesota. The witness reported
that he did not think the pilot intended to takeoff.
He reported the pilot was taxiing on runway 34 when
the wind caught the left wing of the airplane and
it lifted off the runway. The witness reported the
airplane turned sharply to the right and headed
to the southeast. He reported the airplane had difficulty
climbing, but it cleared the trees. Then the airplane
turned into the wind and climbed to approximately
125-150 feet agl. The witness reported the airplane
was making very little forward progress and that
it "hovered" for approximately 15 to 20 seconds.
The airplane then turned downwind. The witness reported
the airplane stalled, but did not spin. He reported
the airplane stalled and "pancaked" into the ground.
The airplane wreckage came to rest about 175 feet
from the initial point of impact.
The witness reported the surface winds were about
12-15 knots out of the west and the wind above the
trees was about 40 knots out of the northwest. He
reported that he was not allowing his flight students
to fly solo because of the high winds.
At 1415, the observed weather was: winds 350
degrees at 10 knots, winds variable from 270 degrees
to 020 degrees, 10 statute miles visibility, sky
clear, temperature 2 degrees C, dew point -7 degrees,
altimeter 29.75.
The pilot of the airplane did not hold a pilot
s certificate or student pilot certificate. The
pilot had applied for a Third Class Medical Certificate
and Student Pilot Certificate, but was denied. The
pilot had been receiving flight instruction prior
to applying for the medical certificate, but discontinued
receiving instruction after being denied the medical
certificate. The pilot s flight logbook was not
recovered and it is uncertain how much flight time
the pilot had acquired.
A witness reported the pilot had received about
20-25 hours of dual flight instruction in a Cessna
172. He reported the pilot had not been endorsed
for solo flight because he did not have a medical
certificate. The witness reported the pilot had
not received any flight training in a tailwheel
airplane. A witness reported the pilot had recently
purchased the airplane and had flown it about three
times.
The airplane was an experimental Wolter Avid
Flyer, Model A, manufactured in 1994. The empty
weight was 450 pounds and the maximum gross weight
was 1,000 pounds. The engine was a 65 horsepower
Rotax 532 engine. The hobbs meter read 233.3 hours
at the accident site.
At the time of the accident, the airplane was
found with the original N number painted over, and
another number painted on the side of the airplane.
A witness reported the pilot had purchased the airplane
about a month prior to the accident flight.
An autopsy was performed. A Forensic Toxicology
Fatal Accident Report was performed by the FAA Civil
Aeromedical Institute. The results indicated that
Verapamil and Norverapamil were detected in the
urine, kidney, and liver. Verapamil is used in treating
coronary artery disease.
The FAA was a party to the investigation.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The unqualified pilot inadvertently stalled the
airplane. A factor was the unqualified pilot s lack
of total experience.
Source: National Transportation Board
Aircraft:
Wampole Mini-Max
Where: Adelanto, Calif.
Injuries: 1 fatal
Phase of Flight: In
flight
About 10:00 Pacific Standard Time, an unregistered
and non-certificated airplane collided with terrain
on El Mirage dry lake near Adelanto, California.
The owner was operating the airplane under the provisions
of 14 CFR Part 91. The non-certificated pilot sustained
fatal injuries; the airplane sustained substantial
damage. The origin point, destination, and purpose
of the flight were not determined. Visual meteorological
conditions prevailed, and no flight plan had been
filed.
Witnesses stated that the airplane was flying
eastbound over the middle of the lake bed about
200 feet agl at 60 to 80 mph. It started to climb;
the right wing suddenly went down, and the airplane
went straight down into the ground. Two of the witnesses
rode their motorcycles to the site, but reported
that the pilot was unresponsive. The sheriff s report
noted that the airplane was a red, white, and blue
"Mini-Max" low wing airplane, but it had no registration
numbers. The right wing was nearly intact. The right
wing was lying against the fuselage with the leading
edge on the ground, and the trailing edge facing
toward the sky. It had ripped from its attachment
point beneath the pilot s seat. The left wing was
destroyed. The landing gear seemed intact except
for the right main landing gear strut, which was
damaged, but still attached. The Rotax engine broke
away from the engine mount. One propeller blade
was shattered and missing; the other blade appeared
undamaged. The fuselage was relatively intact aft
of the cabin. The cockpit sustained severe damage;
its wooden structure was splintered, and almost
unrecognizable as a cockpit.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
A loss of control for undetermined reasons.
Source: National Transportation Board
Aircraft:
Zenair
Where: Kissimmee,
FL
Injuries: None
Phase of flight: Landing
A Zenair 601 experienced a loss of directional
control on landing rollout at Kissimmee Municipal
Airport, Kissimmee, Florida, and crashed. Visual
meteorological conditions prevailed and no flight
plan was filed. The airplane sustained substantial
damage. The private pilot and one passenger reported
no injuries. The flight originated from Winter Haven,
Florida, (GIF) about 1 hour 8 minutes before the
accident.
The private pilot stated he departed GIF on a
local flight and became disoriented as it was beginning
to get dark. He went on guard frequency and attempted
to get some help. He could not locate his position.
He observed a city in the distance, and flew towards
the city. He figured it would have an airport. As
he approached the city, he saw a runway and entered
left base without contacting the control tower.
He lost directional control of the airplane on touchdown.
The airplane went off the side of the runway and
collided with a barricade.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The pilot s failure to maintain directional
control on landing resulting in the airplane going
off the side of the runway and colliding with a
barricade.
Source: National Transportation Board
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