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Aircraft:Beech
23
Where:Macon, GA
Injuries:2 fatal
Phase of Flight:Takeoff
At 1445 Eastern Standard Time, a Beech 23 collided
with trees and subsequently the ground, and burst
into flames while maneuvering for an emergency landing
following a reported loss of engine power near Macon,
Georgia. The personal flight was operated by the
pilot under the provisions of Title 14 CFR Part
91 with no flight plan filed. Visual weather conditions
prevailed at the time of the accident. The airplane
was destroyed, and the private pilot and his passenger
received fatal injuries. The flight departed the
Herbert Smart Airport in Macon, Georgia, at 1443.
According to witnesses located at the departure
airport, the two pilots were last seen at the ready
line for an east departure at the departure airport.
No further visual contact was observed until the
airplane was next seen colliding with trees about
one mile east of the airport. According to the witnesses,
the engine was heard sputtering, followed by the
in-flight collision with 100-foot trees. During
the collision, the right outboard wing panel was
torn from the airframe; the witnesses observed the
airplane as it started a free-fall to the ground.
According to two young eyewitnesses located adjacent
to the accident site, approximately five seconds
after the airplane collided with the ground, it
burst into flames.
PERSONNEL INFORMATION
The pilot held a private pilot certificate with
an airplane single-engine rating. According to Federal
Aviation records, the pilot had accumulated a total
of 83 flight hours, however the pilot flight logs
were not recovered for examination. The pilot's
total flight time in the Beech 23 was not determined.
The pilot held a third class medical certificate,
valid when wearing corrective lens.
AIRCRAFT INFORMATION
The Beech BE-23 was owned and operated by the pilot.
It was a low-wing airplane powered by a Lycoming
O-320-D3B engine. The airframe maintenance logs
were not recovered for examination. However, according
to a work order recovered from Macon Aviation in
Macon, Georgia, the annual inspection was completed.
Macon Aviation did not record the aircraft total
time on the work order. The invoice also showed
that AD 99-05-13 (Airworthiness Directive) was accomplished
during the annual inspection. Additionally, the
work order did not address AD-75-01-04 which specifically
address part number 169-920000-59 which is the fuel
selector installed in the airplane at the time of
the accident. AD-75-01-04 is a recurring inspection
which checks the shutoff characteristics of the
fuel valve. The examination of the fuel selector
valve revealed that it was fire damaged and it was
in the shutoff position at the accident site.
According to refueling records, the airplane
was last refueled at Macon Aviation with 11.6 gallons
of aviation fuel.
METEOROLOGICAL INFORMATION
The 1453 Macon weather observation reported surface
winds at sky clear, visibility 10 miles, wind 020
degrees at four knots. The temperature and dew points
were 60 degrees and 40 degrees respectively. The
altimeter reading was 30.21 inches. According to
icing probability curves, weather conditions were
favorable for the formation of carburetor ice.
WRECKAGE AND IMPACT INFORMATION
Examination of the accident site disclosed that
wreckage debris was scattered over an area 120 feet
long and 40 feet wide. The main wreckage rested
120 feet east of the freshly broken tree branches.
The right outboard wing panel rested 116 feet west
of the main wreckage. Further examination of the
airplane wreckage revealed that the nose and center
sections of the airframe sustained heavy fire damage.
The wreckage path was orientated on a 120-degree
magnetic heading.
During the onsite examination of the airframe,
the extremities of the airframe were located in
the immediate vicinity of the wreckage path. The
right wing panel, with the flap assembly attached,
rested against a tall freshly broken tree along
the wreckage path. A small, fire damaged area was
located approximately mid-span the wing. The main
wreckage, which included the fuselage, empennage,
left wing, and the engine assembly was orientated
on a 280 degree magnetic heading. The fire damage
extended aft through the vertical fin and laterally
through the left wing tip. The grass surrounding
the wreckage was burned throughout the entire width
and length of the wreckage path.
The subsequent wreckage examination showed that
the accessory section of the engine assembly had
melted and was fire damaged. All accessory components
normally installed on the rear of the engine were
also fire damaged. The carburetor assembly also
sustained internal and external fire damage; the
composite float assembly in the carburetor bowl
was heat stressed.
The propeller assembly remained attached to the
engine. Examination of the propeller blades showed
some deformation to the bladed. There were several
freshly broken tree branches in the immediately
vicinity of the right wing assembly. There were
also several branches with diagonal slashes completely
through the diameter of the branch.
The airframe and engine examinations failed to
disclose a mechanical malfunction or component failure.
MEDICAL AND PATHOLOGICAL
INFORMATION
The toxicological examinations revealed 12% carbon
monoxide level in the blood and 0.3 (ug/ml) cyanide
was detected in the blood. The toxicology examination
also revealed 0.083 (ug/ml) of meclizine in the
blood specimens. Meclizine is described as a prescribed
or over-the-counter sedative.
The toxicological examination was negative for
alcohol.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The loss of engine power for undetermined
reasons. A factor was conditions favorable for the
formation of carburetor ice.
Source: NTSB
Aircraft:Beech
BE-23-24
Where:Delaware, OH
Injuries:3 fatal,
1 injury
Phase of flight:Approach
A Beech BE-23-24 was substantially damaged during
a forced landing near Kingston, Ohio. The certificated
airline transport pilot and two passengers were
fatally injured. A third passenger was seriously
injured. Night visual meteorological conditions
prevailed for the personal flight that departed
Burke Lakefront Airport (BKL), Cleveland, Ohio;
destined for Ohio State University Airport (OSU),
Columbus, Ohio. No flight plan was filed and the
flight was conducted under 14 CFR Part 91.
Earlier that evening, the airplane departed Columbus
at 1747, and flew to BKL, arriving at 1841. There
was no record of the airplane being fueled while
at BKL. The airplane then departed at 2130. Once
airborne, the pilot contacted air traffic control
and requested radar traffic advisories. A transponder
code was assigned and the flight progressed with
no report of difficulty. Once in the Columbus area,
the airplane was handed-off to Columbus Approach
Control, and at 2228, the pilot reported starting
a descent from 6,500 feet msl.
Approximately 4 minutes after initiating a descent,
the pilot reported a rough running engine, and requested
vectors to the nearest airport. The controller advised
the pilot that Delaware Municipal Airport (DLZ),
Delaware, Ohio, was the closest airport at 265 degrees.
The pilot acknowledged the transmission, and declared
an emergency. The controller added that the airport
was 13 miles away. At 2235, another pilot over Delaware
reported the runway lights were on at the airport.
The controller confirmed with the accident pilot
that he had received the transmission. The accident
pilot acknowledged the transmission, adding that
he did not see the lights. At 2236, the controller
advised the pilot he was about 12.5 miles from the
runway. The pilot replied he would not make the
airport, adding the engine was not even maintaining
1,000 rpm.
After receiving this transmission, the controller
requested assistance from a Columbus Police Helicopter
that was approximately 12 miles to the southwest.
The helicopter pilot asked the location of the airplane,
and radar vectors were provided. The controller
advised the pilot that a police helicopter was en
route. The pilot replied they were heading towards
the interstate highway. This was the last transmission
received from the accident airplane. Several minutes
later, the helicopter pilot reported seeing traffic
backed-up on the four-lane highway.
The accident happened during the hours of darkness.
PILOT INFORMATION
The pilot held an airline transport pilot certificate
with a multi-engine-land rating, and a commercial
pilot certificate with a single-engine-land rating.
In addition, he held a certified flight instructor
rating for airplane single-engine-land, multi-engine-land,
and airplane instrument. According to the pilot's
latest logbook, he had 2,489.6 hours of total flight
experience with 2,267.6 hours of that in single-engine-land
airplanes. In addition, his logbook reflected that
his last flight in the accident airplane make and
model was about six months before the accident.
During the 30-day window that preceded the accident,
the pilot flew a total of 28.8 hours. In the 60-day
window he flew 58.7 hours, and in the 90-day window
he flew 100.2 hours. All of the flight time logged
by the pilot during the 30, 60, and 90-day windows
was in a Cessna 208B.
AIRCRAFT INFORMATION
According to the Pilot's Operating Handbook (POH),
the airplane was a single engine, low wing, with
fixed landing gear. It was primarily constructed
of aluminum, and could seat up to four occupants.
The airplane was capable of carrying 59.8 gallons
of fuel. To facilitate partial fueling of the airplane,
each of the two fuel tanks was equipped with a visual
indicator called a 'tab.' Then both fuel tanks were
fueled to the base of the 'tabs,' the airplane would
have a total of 30 gallons of fuel onboard, with
approximately 1 gallon unusable.
According to performance data in the POH, on
a standard day, the airplane would use 9.1 gph of
fuel at 63 percent power and 6,500 feet. At 75 percent
power, the airplane would use 12.3 gph of fuel.
The POH also stated that start, run-up, taxi, and
the takeoff acceleration, would require about 0.8
gallons of fuel. According to the preflight inspection
section of the POH, the pilot was required to check
the quantity of fuel in each tank, and to ensure
that the filler caps are secure.
METEOROLOGICAL INFORMATION
At 2251, Port Columbus International Airport, Columbus,
Ohio, (CMH) reported wind 160 degrees at 3 knots,
visibility 10 miles, clear skies, temperature 55
degrees Fahrenheit, dew point 48 degrees Fahrenheit,
and an altimeter setting of 30.13 inches of mercury.
WRECKAGE AND IMPACT INFORMATION
The wreckage was examined at a recovery facility
in Sunbury, Ohio. Both the left and right wings
were attached to the fuselage, along with the horizontal
stabilizer and the vertical stabilizer. All the
flight control surfaces were accounted for, including
the flaps. The majority of the impact damage was
confined to the engine compartment, and the forward
portion of the cockpit area. Flight control continuity
was verified from each of the control surfaces to
the pilot station, and elevator trim was approximately
neutral.
The fuel selector was set to the left tank. Approximately
1/16 of a gallon was drained from the left tank.
The left tank fuel line fitting was broken consistent
with impact damage. Approximately 1/8 of a gallon
of fuel was drained from the right fuel tank. In
addition, approximately 3 oz. of fuel was drained
from the gascolator. A trace amount of fuel was
recovered from the fuel line that connected the
engine driven fuel pump to the airframe, and less
than a teaspoon of fuel was recovered from the engine
driven fuel pump. A trace amount of fuel was recovered
from the line that connected the engine driven fuel
pump to the fuel injector. The fuel screen was removed
from the injector. No contaminates were identified,
and a trace of fuel was recovered. The fuel injector
was removed and held upside down. A trace of fuel
was recovered. The fuel line that connected the
fuel injector to the fuel manifold was removed,
and no fuel was recovered. The manifold was opened
and no fuel was found. In addition, no fuel was
found in any of the four injector-lines. All four
injectors were removed and no obstructions were
identified.
Approximately 15 gallons of water was added to
the right fuel tank. The fuel selector was set to
the right tank, and electrical power was applied
to the electric fuel boost pump. The pump activated,
and water was expelled from the fuel bulkhead fitting
at the firewall. Power to the electric fuel boost
pump was removed, and the fuel selector was repositioned
to the left tank. Because the left tank fuel line
fitting had broken, the left inboard fuel tank feed
line was submerged in a container of water. Again,
electrical power was applied to the electric fuel
boost pump. The pump activated and water was expelled
from the fuel bulkhead fitting at the firewall.
Examination of the engine and accessories revealed
that the engine driven fuel pump had partially separated
from the engine. The pump was removed and disassembled.
No pre-impact failures were identified. The vacuum
pump was removed, and the sheer coupling was intact.
The pump was disassembled, and the vanes and vane
housing were intact. All of the spark plug electrodes,
except for two, were grayish in color. The number
2 cylinder bottom sparkplug could not be removed
because of impact damage, and was not examined.
The number 1 cylinder bottom sparkplug electrode
was covered in non-combusted oil.
A rotational force was applied to the engine
crankshaft. Thumb compression was obtained on all
four cylinders and spark was observed on all eight
magneto-towers. Continuity of the ignition leads
could not be verified because of impact damage.
In addition, the engine driven fuel pump pad articulated,
and the vacuum pump pad rotated.
ADDITIONAL INFORMATION
According to the owner of the recovery company that
removed the airplane from the interstate highway,
there was no evidence of spilled fuel on the road
were the airplane came to rest, nor did he find
any fuel on the bed of the truck used to move the
airplane. He added that besides not seeing any fuel,
he did not detect the aroma of fuel.
According to the president of the flying club
that owned the airplane, the pilot went to work
for a cargo company flying a Cessna 208B. After
that, the pilot did not rent the accident airplane,
or one of the same make and model. In addition,
the president flew the accident airplane the day
before the accident with a student. Before the flight,
the president's student estimated the left tank
had approximately 7 1/2 gallons of fuel, and the
right had 15 gallons. The student also noted that
his observation matched the fuel quantity gauges.
The president then flew the airplane for about 1.3
hours. After the flight was completed, the airplane
was not serviced until the next day when the accident
pilot requested it be fueled to the 'tabs.'
An interview was conducted with the line attendant
that serviced the airplane at Columbus. The attendant
was asked to complete a written statement, and was
advised he would be asked a few questions afterwards.
According to the attendant, he received a fuel
order around 1745, to fuel both tanks to the 'tabs'
on the accident airplane. After fueling the tanks
to the 'tabs,' he replaced the fuel caps. He then
watched the pilot open the left fuel cap, and check
the fuel level. The pilot told the attendant he
was surprised it only took 13.2 gallons to service
the airplane. The attendant added that the airplane
was on level terrain when it was serviced, and that
he only remembered seeing the pilot check the left
fuel tank.
In a statement given to an Ohio State Trooper, the
passenger that survived the accident stated she
did not remember seeing the pilot visual check either
fuel tank while the airplane was in Cleveland. She
added that right before the accident, the pilot
started getting 'nervous,' and then the airplane
went 'crazy.'
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows. The pilot's failure to check both fuel
tanks visually during the preflight inspection.
A factor in the accident was the dark night.
Source: NTSB
Aircraft:
Beech 24R
Where: Wauseon, Ohio
Injuries: 3 fatal
Phase of Flight: landing
At 1510 eastern daylight time, a Beech 24R was
substantially damaged while attempting to land at
Fulton County Airport (USE), Wauseon, Ohio. The
certificated airline transport pilot and the two
passengers were fatally injured. No flight plan
was filed for the flight that originated at Oakland-Troy
Airport (7D2), Troy, Michigan, about 1415. Visual
meteorological conditions prevailed for the personal
flight conducted under 14 CFR Part 91. The pilot,
along with his wife and daughter, flew from Minnesota
to Troy to attend a wedding the following day.
According to the general manager of a fixed base
operator at Oakland-Troy Airport, on the day of
the accident, the pilot arrived with his family
shortly before 1330, and requested that the airplane
be filled with fuel. While the airplane was being
fueled, the pilot asked if anyone had flown that
day, and if so, did they talk about the weather
conditions. The general manager replied that due
to the "very, very windy" weather conditions, few
people had flown that day, except for a Mitsubishi
MU-2. He did not think the pilot would fly that
day based on the wind conditions, which he estimated
to be from the west-southwest about 40 miles per
hour.
After paying for the fuel, the pilot went to
the terminal building to use the Weather Data Inc.,
computer. Approximately 30-40 minutes later, he
returned to the FBO, and prepared the airplane for
flight.
A witness, a certificated pilot who reported
over 1,000 hours of flight time, said he was at
his parents' house about 3 miles east of Fulton
County Airport, when he heard a "normal aircraft
sound" fly overhead from east to southwest; at an
altitude of approximately 1,000 feet, between 1510
and 1515. As the airplane flew overhead, he made
the comment, "Who would be out in these winds?"
He left his parents' house at 1530, and did not
learn about the accident until later that day.
A review of radar data revealed that a target
emitting a visual flight rules (VFR) transponder
beacon code approached Fulton County Airport from
the northeast. The last 2 1/2 minutes of radar data
revealed that the target turned west and tracked
toward runway 27. During that time, the target descended
from 1,900 feet msl to 900 feet msl, before the
data ended at 1909:52. The last radar return was
located approximately 0.19 miles from the end of
the runway, at a ground speed of 68 knots. The elevation
of the airport was 779 feet msl.
The wreckage was located about 1545, by an individual
who was driving on a road perpendicular to the runway.
The accident occurred during the hours of daylight,
approximately 41 degrees, 36 minutes north latitude,
and 84 degrees, 07 minutes west longitude.
PILOT INFORMATION
The pilot held an air transport pilot certificate
with a rating for rotorcraft-helicopter. He also
held a commercial certificate with ratings for airplane
single engine land, and instrument airplane. His
most recent Federal Aviation Administration (FAA)
third class medical was issued on August 14, 2001.
Examination of the pilot's logbook revealed that
he had a total of approximately 4,113 flight hours,
of which, 14 hours were in the last 90 days.
A certified flight instructor had given the pilot
1.7 hours of flight instruction in the airplane
on May 8, 2003. Examination of flight logs revealed
the pilot had accrued a total of approximately 7
hours in make and model at the time of the accident.
METEOROLOGICAL INFORMATION
Weather reported at Toledo Express Airport (TOL),
Toledo, Ohio, about 14 nautical miles west of Wauseon,
at 1452, included winds from 240 degrees at 33 knots
gusting to 45 knots, visibility 10 statute miles,
scattered clouds 4,200 feet, overcast clouds 5,500
feet, temperature 59 degrees F, dew point 41 degrees
F, and a barometric pressure of 29.50 inches Hg.
An urgent weather message, which was issued by
the National Weather Service at 1202, and expired
at 2000, included Wauseon, Ohio. According to the
message:
"An intense low pressure system over the upper Great
Lakes will cause strong southwest to west winds
across southern Michigan...northern Indiana...and
northwest Ohio today. Winds will be sustained at
25 to 35 mph with gusts of 45 to 55 mph much of
the day.
A wind advisory is issued when sustained winds
of 30 mph or greater are expected for at least an
hour or wind gust of 45 mph or greater occur at
any time. Without extra precautions these winds
may cause minor property damage. Motorists in high
profile vehicles should exercise great care."
The manager of the Fulton County Airport stated
that the wind conditions at the airport at the time
of the accident were from the west, southwest between
30-40 mph and gusting to 40-50 mph.
Runway 27 was a 3,882-foot-long and 75-foot-wide
asphalt runway with 80-foot trees located on the
north and south sides of the first third of the
runway. The trees on the north side of the runway
were about 200 feet from runway centerline, while
the trees on the south side of the runway were about
550 feet from runway centerline. The airport manager
described turbulence that occurred at times between
the two sections of trees as a "terrible, terrible
funnel effect...with lots of rolling wind."
WRECKAGE INFORMATION
The wreckage was examined at the site. All major
components and all flight control surfaces were
accounted for at the scene. The wreckage was located
off airport property, in a muddy, barren cornfield,
about 350 feet north of the approach end of runway
27.
The airplane came to rest upright, the nose gear
was separated, and both wings remained partially
attached to the fuselage. The cockpit area was crushed,
and there was no post-impact fire.
The wreckage path measured 100 feet from the
initial ground scar to the main wreckage, and was
oriented 358 degrees magnetic. The airplane came
to rest oriented 240 degrees magnetic.
The initial impact point was a ground scar, where
broken pieces of green navigational lens were found
imbedded. Also found along the wreckage path were
the right wing tip, landing light, nose landing
gear, and the lower and upper section of the engine
cowling.
Examination of the airplane revealed that the
left main landing gear was extended, and the right
main landing gear was retracted. The landing gear
selector handle was broken and in the "up" position.
Control cable continuity was established for
each of the flight control surfaces to the cockpit.
Examination of the flap actuator jack screw revealed
that the flaps were fully extended.
The left wing fuel tank was full and the right
wing fuel tank was partially filled with blue-colored
fuel. The fuel selector valve was found set to the
right tank.
The engine was intact, but exhibited impact damage,
and all three propeller blades remained attached
to the propeller hub. The first blade was straight
and exhibited some front face polishing. The second
blade was bent slightly aft and also exhibited front
face polishing. The third blade was bent aft and
exhibited front face polishing and trailing edge
nicks near the tip.
The top and bottom spark plugs were removed,
and appeared light gray in color.
The fuel injector nozzles were removed and examined.
The nozzles were absent of debris, except for the
#1 nozzle.
All of the fuel lines were intact and secure.
Fuel was present at the fuel pump, injector, and
flow divider.
The fuel servo filter screen was removed and
found absent of debris. In addition, a small amount
of fuel was found in the firewall fuel strainer
bowl, and the filter was absent of debris.
Valve train continuity and compression in each
cylinder were confirmed by manual rotation of the
propeller flange. While the engine was being rotated,
spark was produced to each ignition lead, except
the #3 bottom due to the harness being torn. The
harness was then manually cut at the terminal, the
engine was rotated again, and spark was observed.
The oil suction screen was removed and examined.
The only debris noted was an inch-long, thin piece
of sealant.
MEDICAL AND PATHOLOGICAL INFORMATION
An autopsy was performed on the pilot by the
Lucas County Coroner's Office, Toledo, Ohio. Toxicological
testing was performed by the FAA Toxicology Accident
Research Laboratory, Oklahoma City, Oklahoma.
ADDITIONAL INFORMATION
A review of fueling records revealed that the
airplane was fueled with 37.3 gallons of 100 LL
fuel on the day of the accident, which filled the
tanks.
The airport manager reported that the airport
commission, along with state and local government,
had been working for several years to have the trees,
which were located on private property, removed.
A review of the Airport/Facility Directory revealed
that there were no remarks, which warned pilots
of the possible encounter with turbulence when landing
on runway 27.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain control during the
approach-to-landing. Factors were the high wind
gusts and turbulence, and the pilot's decision to
fly in those weather conditions.
Source: NTSB
Aircraft: Beech C24R
Where: Virginia Beach, VA
Injuries: 2 fatal
Phase of flight: Landing
A single-engine Beech C24R airplane sustained substantial damage when it collided with trees and terrain following a loss of control while attempting to return to land on Runway 32 at the Norfolk International Airport (ORF), near Norfolk, Virginia. The instrument rated private pilot, his passenger, and two dogs sustained fatal injuries. An instrument flight rules (IFR) flight plan was filed for the cross-country flight destined for the Hilton Head Island Airport (HXD), near Hilton Head, South Carolina. Visual meteorological conditions prevailed for the personal flight conducted under 14 Code of Federal Regulations Part 91.
A review of the air traffic control communications revealed the flight was cleared for take-off on Runway 32 (a 4,875-foot-long, by 150-foot-wide asphalt runway) at 1127:04. Shortly after takeoff, the 1,493-hour instrument rated private pilot informed air traffic control that a "door had opened" and that he needed to return to the airport. A tower controller then instructed the pilot to turn left and enter the downwind leg of the traffic pattern for Runway 32, and the pilot acknowledged. The controller then asked the pilot if he was able to make a short approach, to which the pilot replied that he could. The controller then cleared the pilot to land on Runway 32. A few moments later, the tower controller advised the pilot to extend the downwind leg due to traffic on final approach, and that the tower would inform him when he could turn onto the base leg. The pilot again acknowledged the radio transmission. At 1129:43, the tower controller instructed the pilot to turn onto the base leg, and again, the pilot acknowledged. This was the last radio communication received from the pilot.
A review of the radar data indicated the airplane departed runway 32 and leveled-off at an altitude of 200 feet mean sea level (msl), while maintaining a ground speed of 100 knots. Radar data revealed that the airplane executed a left turn to a southeasterly heading and flew parallel to the runway. Radar data also revealed that as the airplane proceeded on this heading, its ground speed decreased to 70 knots. When the airplane was about one-mile beyond the end of the runway, another left turn was initiated toward the northeast before the radar data ended at 1130.
A witness, who was working in his garage, reported that he heard "a large shaking sound which sounded like a semi-type truck braking down in front of [his] house." The witness then looked up and saw the airplane flying "very slow" about 20-feet-high above the tree line. The airplane was shaking and it sounded like it was losing power. The witness was provided a model airplane to demonstrate the flight attitude of the airplane. The witness demonstrated that the airplane had a slightly nose-high attitude and was in a shallow left hand turn. The airplane was shaking violently. The witness then maneuvered the model airplane so it simultaneously rolled rapidly to the left (inverted) and the nose of the airplane dropped toward the ground. The witness further stated that he lost sight of the airplane as it descended into the trees.
The aircraft stalled while in the traffic pattern and struck trees, then crashed into the ground.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's failure to maintain airspeed, which resulted in an inadvertent stall/spin while maneuvering at a low altitude. Contributing was the pilot's diverted attention to an open door.
Source: National Transportation Board
Aircraft: Beechcraft F33A
Where: Buckeye, AZ
Injuries: 1 fatal
Phase of flight: Landing
After crossing flight paths with a military fighter jet, the single engine airplane entered an increasingly steep descent and subsequently impacted terrain. The student pilot was flying her third solo flight of the flight-training syllabus. The ATCA solo flight order authorized the student to depart from Phoenix Goodyear airport, fly to Buckeye Airport, perform at least one landing, taxi back, takeoff, then proceed to a practice area south of the Phoenix Goodyear Airport, perform steep turns, slow flight, and stalls, and finally return to Phoenix Goodyear Airport. The student was reported as overdue at 1615. Five aircraft were launched to search for the overdue airplane at 1640. The Maricopa County Sheriff Department helicopter located the wreckage on at 0040 in flat desert terrain 12.5 miles south-southeast of the Buckeye Airport.
The solo student pilot departed the airport and proceeded to climb towards a designated practice area. Upon reaching 4,500 feet the pilot reduced power and entered a 500-foot-per-minute descent. At this point the pilot may have been alerted by the on-board TCAS (traffic/collision alerting device) that there was traffic approaching from her right side, close to her altitude. The sun was also off her right side at an elevation of 31 degrees above the horizon. Within seconds an F-16 fighter jet crossed in front of her from right to left. The closest point of approach between the two aircraft, as determined by a radar data study, was 1,850 feet laterally and 400 feet vertically. A study of the wake and vortex turbulence that would have been produced by the F-16 determined that the generated vortices could not have dropped low enough to affect the path of the student's airplane. After the F-16 passed, the student's airplane continued an increasingly steep linear descent, eventually exceeding 2,500 feet per minute before impacting the terrain at a 50-degree nose down, right wing down attitude, 29 seconds after the encounter. Multiple close examinations of the aircraft wreckage failed to reveal any evidence of mechanical failure or malfunction. A review of the student's available medical records, autopsy, and toxicology analysis did not reveal any physiological inconsistencies. It is certainly possible (and consistent with the circumstances of the accident) that the student pilot lost consciousness following her presumed near collision; however, there is not enough information available to fully support this hypothesis.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The student pilot's failure to maintain aircraft control for undetermined reasons.
Source: National Transportation Board
Aircraft:
Beech 35-A33
Where:Heber City,
UT
Injuries:1 Fatal
Phase Of Flight:Maneuvering
A Beech 35-A33 impacted terrain while maneuvering
about 10 nautical miles north of Heber City, Utah.
The non-instrument rated commercial pilot, the sole
occupant, was fatally injured, and the airplane
sustained substantial damage. The airplane was registered
to and operated by the pilot. A visual flight rules
(VFR) flight plan was filed for the personal cross-country
flight conducted under 14 CFR Part 91. The airplane
departed Billings, Montana, about 0910 with an intended
destination of Spanish Fork, Utah. Visual meteorological
conditions prevailed for the departure from Billings,
and instrument meteorological conditions prevailed
at the accident site.
According to information provided by Salt Lake
City Air Route Traffic Control Center (ARTCC), the
flight was receiving VFR flight following services.
About 1119, the controller working the flight advised
the pilot that there was a storm system in the Salt
Lake valley and to the south. The pilot acknowledged
receiving the information. About 1138, the pilot
was again advised of deteriorating weather conditions
along his route of flight. Again, the pilot acknowledged
receiving the information. About 1151, the pilot
reported that he was over Evanston, Wyoming, at
8,000 feet mean sea level (msl), following I-80
south, and that if needed, he would turn around
and land at Fort Bridger, Wyoming. About 1209, relaying
through another aircraft, the pilot was informed
that radar contact was lost. About 1214, again relaying
through another aircraft, the pilot reported that
he planned to go through "either Heber City or Provo
canyon." About 1217, another relay was attempted
to inform the pilot about level 2 and 3 precipitation
in those canyons, and no reply was received. Several
other attempts were made to relay without success.
Further attempts were made to contact the airplane,
and no reply was received.
Radar data provided by Salt Lake City ARTCC indicated
that radar contact with the airplane was lost about
1206. The last minute of continuous recorded radar
data shows the airplane proceeding southbound along
I-80 near the town of Wahsatch, Utah, located about
37 nautical miles north-northeast of the accident
site. Between 1204:45 and 1205:45, the airplane
traveled a distance of 2.6 miles, consistent with
a ground speed of approximately 135 knots, and descended
from 7,300 to 7,100 feet msl. (The elevation of
Wahsatch is 6,742 feet.)
A witness, who was a private pilot, reported
to the NTSB investigator-in-charge (IIC) that about
1215, he observed a single-engine, retractable gear
airplane flying south along I-80 through the town
of Coalville, Utah, located about 16 nautical miles
north of the accident site. The witness stated the
ceiling was about 500 feet, and there was light
snow and sleet falling. He estimated the airplane
was about 300 feet above ground level (agl), "going
fairly slow," about 100 to 120 mph. He later saw
pictures of the accident airplane and realized it
was the same airplane he had seen.
A witness reported to the Summit County Sheriff's
Office that at 1226, she was near mile marker 2
on State Road 40, located about 4 nautical miles
north of the accident site, and observed a "white
plane with what she thought were red letters" flying
overhead. (The accident airplane was painted white
with blue and red trim.) According to the witness,
"it was snowing hard and there was little visibility."
The airplane was heading south, following State
Road 40, "flying low" at an altitude of "approximately
300 feet off of the ground."
At 1229:02, one radar return was recorded from
the airplane. This last return showed the airplane
located approximately 1/2 mile north of the accident
site at an altitude of 7,000 feet msl.
According to a report prepared by the Summit
County Sheriff's Office, at 1230, the Summit County
Dispatch Center received an emergency call in regards
to a low flying airplane near mile marker 8 on State
Road 40. At the time of the call, officers working
in the area were unable to locate the low flying
airplane. They reported that "the weather in the
area was extreme. Visibility was less than 500 feet
with heavy snow." About 1530, Summit Dispatch received
a report that an airplane was down near mile marker
6 on State Road 40. The caller advised that the
airplane was approximately 500 feet east of the
roadway. Officers responded to the scene and identified
the airplane as N1254Z.
PERSONNEL INFORMATION
The pilot held a commercial pilot certificate
with an airplane single engine land rating. He did
not hold an instrument rating. His most recent medical
certificate was a second class medical, with the
limitation, must wear corrective lenses. On the
application for this medical certificate, the pilot
reported that he had accumulated 1,090 hours total
flight time. The pilot's flight logbooks were not
examined during the investigation.
AIRCRAFT INFORMATION
Examination of the airplane's maintenance records
indicated that the 1961 model Beech Debonair received
its most recent annual inspection at a total time
of 3,823.2 hours. As of that date, the engine, a
Continental IO-470-K, S/N 86029, had accumulated
394.5 hours since major overhaul. Review of the
maintenance records revealed no evidence of any
uncorrected maintenance discrepancies.
METEOROLOGICAL INFORMATION
The following weather conditions were reported
at Heber City, Utah, located approximately 10 nautical
miles south of the accident site, elevation 5,637
feet:
At 1155, wind from 320 degrees at 7 knots, visibility
2 1/2 statute miles, rain, sky conditions: broken
clouds at 1,600 feet, overcast at 2,300 feet, temperature
2 degrees C, dew point 1 degree C, and altimeter
29.83 inches.
At 1255, wind from 280 degrees at 3 knots, visibility
7 statute miles, light rain, sky conditions: scattered
clouds at 1,700 feet, broken clouds at 3,300 feet,
overcast at 4,200 feet, temperature 2 degrees C,
dew point 1 degree C, and altimeter 29.81 inches.
According to information provided by Cedar City
Automated Flight Service Station (AFSS), at 0741,
the pilot received a weather briefing from Great
Falls AFSS for a VFR flight from Billings, Montana
to Spanish Fork, Utah. The pilot stated that the
flight would take about 3 and 1/2 hours and that
his planned route was "through the basin down to
Lander...then west [to] Fort Bridger...Heber City
then through the Provo canyon." The briefer began
the briefing by stating "for western Wyoming and
the rest of the route airmet for occasional mountain
obscuration, clouds, precipitation, mist and fog,
VFR not recommended into that area." While en route,
the pilot twice contacted Cedar City AFSS, at 1121
and 1140, requested and was given current and forecast
weather conditions along the route from Fort Bridger
to Evanston to Provo. During each contact, he was
told that VFR flight was not recommended along the
route.
WRECKAGE AND IMPACT INFORMATION
Summit County Sheriff's Office personnel examined
the accident site and reported the main wreckage
was located at 40:39.375 North latitude and 11:27.291
West longitude at an elevation of 6,933 feet. According
to the Summit County Sheriff's Office report, when
officers reached the scene about 1600, there was
approximately 1 inch of new snow on the airplane.
The airplane was facing north, and there was a ground
scar marking the initial impact point about 100
feet south of the airplane. Branches were broken
from the oak brush located between the ground scar
and the airplane. The outboard third of the right
wing separated and was found at the initial impact
point.
The wreckage was recovered from the accident
site and moved to the Heber City Municipal Airport.
The wreckage was examined by the NTSB IIC and representatives
from the FAA and Teledyne Continental Motors. The
engine was separated from the airframe. The propeller
remained attached to the engine crankshaft. One
of the blades was bent aft approximately 8 inches
from the propeller hub and exhibited chordwise scratching
and gouging throughout the span of the blade. The
other blade was bent aft and exhibited blade twisting
with chordwise scratching on the outboard 12 inches
of the forward side of the blade. The rocker arm
covers and the top spark plugs were removed. The
engine was rotated by hand using the propeller,
and engine continuity was confirmed. "Thumb" compression
was obtained on all cylinders. Both magnetos sparked
at all leads during hand rotation of the propeller.
The cylinder combustion chambers were examined through
the spark plug holes using a lighted borescope.
There was no visible evidence of foreign object
ingestion or detonation, and the valves appeared
to be intact and undamaged. The fuel pump turned
freely and was not damaged. The fuel pump drive
was intact and undamaged. The fuel manifold valve
was disassembled and the screen was free of debris;
the diaphragm and spring were undamaged. Inspection
of the engine did not reveal any abnormalities that
would have prevented normal operation and production
of rated horsepower.
MEDICAL AND PATHOLOGICAL
INFORMATION
An autopsy of the pilot was conducted by the
State of Utah's Office of the Medical Examiner in
Salt Lake City, Utah. Toxicology tests conducted
by the FAA's Toxicology and Accident Research Laboratory
were negative for carbon monoxide, cyanide, ethanol
and drugs.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's continued VFR flight into IMC and his
subsequent failure to maintain terrain clearance
while maneuvering resulting in an in-flight collision
with terrain. Contributing factors were low ceilings,
snow, and mountainous terrain.
Source: NTSB
Aircraft:
Beech D35
Where: Agua Dulce,
CA
Injuries: 1 fatal
Phase of Flight: Cruise
About 2003 hours Pacific daylight time, a Beech
D35 operated by the pilot, collided with upsloping
mountainous terrain about 3 miles east-northeast
of Agua Dulce, California. The airplane was destroyed,
and the instrument-rated private pilot was fatally
injured. Instrument meteorological conditions prevailed
in the vicinity, and no flight plan was filed for
the personal flight that was performed under 14
CFR Part 91. The flight originated from Santa Paula,
California, approximately 1945.
An acquaintance of the pilot reported to the
National Transportation Safety Board investigator
that upon departure, the pilot intended to fly in
an easterly direction to Chandler, Arizona, where
he was to meet her. No witnesses reported observing
the airplane impact the hillside.
The property owner, onto whose land the airplane
crashed, reported to the Safety Board investigator
that he was home at 2000. He did not observe or
hear the impact, and he did not hear any engine
noise at that time or thereafter. The airplane collided
into the mountainside about 700 feet from his home.
PERSONNEL INFORMATION
A copy of the pilot's personal flight record logbook
was examined. It indicated that he had a total of
approximately 2,072 hours of experience flying airplanes.
During the 90-day period preceding the accident,
the logbook indicated the pilot flew his airplane
for about 57 hours, of which 18 hours were flown
at night.
The pilot was issued an instrument rating in
1983. His total instrument flying experience was
approximately 76 hours, of which 6 hours were logged
as "actual" and 70 hours were logged as "simulated."
No evidence of any instrument competency flight
check or proficiency flying was observed between
1993 and the accident date.
An acquaintance of the pilot reported to the
Safety Board investigator that the pilot had flown
the accident route of flight on many occasions.
Also, he was familiar with the area. The acquaintance
also reported that the pilot worked as an automotive
mechanic
AIRPLANE INFORMATION
No current aircraft maintenance logbook was located.
A written statement was subsequently received from
a Federal Aviation Administration (FAA) certificated
mechanic in which he reported that an annual inspection
was accomplished on the accident airplane. The mechanic
indicated that he had assisted the pilot in performing
the inspection. All airworthiness directives had
been complied with. Also, the pitot-static system
and the transponder check were accomplished.
METEOROLOGICAL INFORMATION
On the date of the accident sunset occurred about
1935 at the accident site. Civil twilight ended
about 2002. No illumination from the moon was present
at 2003.
The nearest airport to the accident site located
south of the San Gabriel Mountains that reported
its surface weather is the Burbank-Glendale-Pasadena
Airport. Burbank's elevation is 775 feet mean sea
level (MSL), and it is located about 18.6 nautical
miles and 179 degrees (magnetic) south of the accident
site. At 1953, Burbank reported an overcast ceiling
at 2,600 feet above ground level, or about 3,375
feet MSL.
A hillside resident located about 1/3-mile downslope
from the accident site reported that at 2000 his
home (approximate elevation 3,200 feet MSL) was
shrouded in ground fog (low clouds). There was no
evidence of precipitation.
According to the FAA, at the time of the accident
low ceilings were forecast for the accident site
area. The FAA reported that the pilot did not file
a flight plan and neither requested nor received
any weather briefing services.
Both of the Direct User Access Terminal (DUAT)
vendors verbally reported to the Safety Board investigator
that a search of their computer transactions failed
to produce any evidence that the pilot (using his
name or airplane registration number) received any
weather briefing services or made any inquiries
on the date of the accident.
AIDS TO NAVIGATION
According to the FAA, all electronic aids to navigation
pertinent to the airplane's route of flight were
functional.
COMMUNICATION
The FAA reported that it had not been requested
to provide any services to the accident pilot/airplane.
WRECKAGE AND IMPACT INFORMATION
The initial point of impact (IPI) occurred on estimated
10-degree upsloping terrain at an elevation of about
3,560 feet mean sea level. The approximate global
positioning satellite (GPS) coordinates of the IPI
are 34 degrees 30 minutes 08.8 seconds north latitude
by 118 degrees 16 minutes 15.3 seconds west longitude.
The main wreckage was found on an adjacent hill
northeast of the IPI, at GPS coordinates of approximately
34 degrees 30 minutes 14.0 seconds north latitude
by 118 degrees 16 minutes 09.0 seconds west longitude.
The approximate magnetic bearing between the
IPI and the main wreckage is 031 degrees. The distance
is about 750 feet.
An examination of the terrain at the IPI revealed
ground scar consistent in appearance with the dimensions
and shape of the airplane. Fragments from the right
and left wing tips were located about 16 feet southeast
and northwest, respectively, from the main impact
crater. Portions of engine cowl were found in the
crater and within 75 feet to the northeast.
The left wing's pitot tube was found on the left
side of the impact crater. One propeller blade was
found about 120 feet upslope from the IPI; the second
blade was found attached to the engine, which had
separated from its airframe attachments, and was
about 75 feet downslope from the main wreckage.
Both propeller blades were observed torsionally
twisted, scratched in a chordwise direction, and
bent into an "S" shape.
The main wreckage was found upside down, on a
heading of about 050 degrees, with the wing flaps
and landing gear retracted. The leading edges of
both wings were observed accordioned in an aft direction.
All of the flight control surfaces were found attached
to the airframe. The continuity of the flight control
system was confirmed between the aft empennage and
the crushed mid-fuselage section. There was no evidence
of oil streaking, sooting, or charred (fire damage)
material in any of the wreckage.
Inside the cabin, various hand tools, plastic
gasoline containers, and associated maintenance-related
equipment were observed.
MEDICAL AND PATHOLOGICAL
INFORMATION
An autopsy was performed by the Los Angeles County
Coroner's Office. Results of toxicology tests on
the pilot were negative for carbon monoxide and
ethanol. Phenylpropanolamine was detected in specimens
from the pilot's blood and urine. This drug is contained
in over-the-counter decongestant and weight loss
medications.
TESTS AND RESEARCH
The engine was examined on scene. The crankshaft
could not be rotated. There was no evidence of oil
leakage onto the external case surface, and no evidence
of soot or heat distress signatures was present
in the vicinity of the exhaust stacks. The sparkplugs
were removed and examined. According to the Continental
engine representative, all observed plugs presented
an appearance consistent with normal wear signatures.
Specifically, the electrodes were dry, and the wear
pattern was normal in appearance.
ADDITIONAL INFORMATION
The accident site is located about 0.5 miles north
of California State Highway 14, which principally
has a northeast to southwest orientation. The accident
site is visible from the highway, which has an elevation
of about 3,000 feet in this area.
The maximum elevation of Highway 14 is reached
in the Soledad Pass. The Pass's elevation is 3,225
feet MSL. This local is about 8 miles east of the
accident site.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain terrain clearance
while cruising up a mountain pass, on a dark night,
in IMC conditions, and his improper in-flight decision
to perform a VFR flight in the inclement weather.
Source: NTSB
Aircraft:
Beech G35
Where: Falmouth,
MA
Injuries: None
Phase of Flight: Taxiing
A Beech G35 was substantially damaged during
a collision with trees while taxiing for takeoff
at Falmouth Airpark (5B6), Falmouth, Massachusetts.
The certificated private pilot and passenger were
not injured. Visual meteorological conditions prevailed,
and no flight plan was filed.
The pilot was interviewed via telephone and submitted
a written statement. He stated that he performed
a preflight inspection of the airplane, then started
the engine while parked on the apron adjacent to
his hangar.
The pilot increased the throttle in order to
start the airplane moving over snow that had accumulated
on the apron and taxiway. He then reduced the throttle
after the airplane began accelerating; however,
the engine continued to run at a higher rpm. The
pilot tried again to reduce the throttle, to no
avail. The airplane continued to accelerate at a
"higher than normal" rate across the taxiway.
The pilot then applied full right rudder pedal
and right brake, but the airplane did not respond,
and continued to slide on the snow. The airplane
impacted a line of trees, on the opposite side of
the taxiway, head-on.
Additionally, the pilot reported that after the
accident he and a friend inspected the throttle
and carburetor. He reported hearing a "snapping
sound" and felt a "binding" of the throttle cable.
The pilot's hanger was located in a residential
area of the Falmouth Airpark. Access to the runway
was provided via a 50-foot wide grass taxiway that
ran perpendicular to the apron immediately in front
of the pilot's hangar. Examination of pictures taken
by the pilot on the day of the accident revealed
that the taxiway and the grass portion of the apron
in front of the hanger were covered with patches
of snow.
The airplane was a 1956 Beech G35, and had accumulated
3,430 total flight hours at the time of the accident.
The airplane's most recent annual inspection was
performed and the airplane had accumulated 64 flight
hours since that time.
The pilot held a private pilot certificate with
a rating for airplane single engine land, and a
third class medical certificate. At the time of
the accident he reported 796 hours of total flight
experience, and 47 hours of flight experience in
make and model.
A Federal Aviation Administration (FAA) inspector
examined the airplane. The inspector found that
the throttle was stiff, but he could only duplicate
the snapping sound heard by the pilot once, and
noted a very slight vibration within the throttle.
The inspector also found that the throttle moved
completely from the idle to the full power position
with no obstruction or hindrance.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain control of the airplane
during taxi. A factor was the snow-covered taxiway.
Source: NTSB
Aircraft:Beech
K35
Where:Fillmore, UT
Injuries: None
Phase of Flight:Climbout
A Beech K35 was substantially damaged when it
collided with terrain during initial climb following
takeoff from Fillmore Airport, Fillmore, Utah. The
private pilot and three passengers were not injured.
Visual meteorological conditions prevailed, and
no flight plan was filed for the business cross-country
flight. The intended destination was St. George,
Utah.
According to the pilot, during takeoff roll on
runway 22, the aircraft was "trimmed incorrect[ly]
and left the runway premature[ly]." The airplane
lifted off the runway, settled back down, and immediately
lifted off the runway again. The aircraft had insufficient
airspeed and the stall warning horn sounded. He
retarded the throttle and the airplane departed
the runway to the left into the grass. The propeller,
cowling and landing gear were bent, and the fuselage
was wrinkled.
When asked what recommendation the pilot could
make as to how the accident could have been prevented,
he stated 'use of a checklist.'
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The pilot's failure to adequately remove
ice and snow from the airplane. A contributing factor
was the pilot's inability to maintain control during
climb due to degradation of the airplane's aerodynamic
performance.
Source: NTSB
Aircraft:
Beech V35B
Where: Bay St. Louis,
MS
Injuries:None
Phase of Flight:Landing
On June 27, 2004, about 0730 central daylight
time, a Beech V35B, N2167L, registered to a private
individual, was landed with the landing gear retracted
at the Stennis International Airport, Bay Saint
Louis, Mississippi. Visual meteorological conditions
prevailed at the time and no flight plan was filed
for the 14 CFR Part 91 personal flight from the
Mobile Downtown Airport, Mobile, Alabama, to the
Stennis International Airport, Bay Saint Louis,
Mississippi. The airplane was substantially damaged
and the private-rated pilot, the sole occupant,
was not injured. The flight originated about 0700,
from the Mobile Downtown Airport.
The pilot stated that the flight proceeded to
the destination airport where he descended to traffic
pattern altitude and entered the downwind leg at
a normal 45-degree entry. When abeam the numbers
during the downwind leg, he placed the landing gear
selector handle to the down position and observed
three green lights. He also reported that the airplane
slowed as though the extended gear drag was present.
The rest of the approach was what he considered
typical and at no time was there any indication
that something was "amiss." After a typical final
approach he reduced power to idle and entered ground
effect, then during the flare approximately 2-5
feet above the runway surface, he heard the gear
warning horn sound but it was not until the propeller
contacted the runway surface did he realize, "...the
gear must not have been locked, or must have cycled
back into the up position." The airplane came to
rest on the right side of the runway. The pilot
further stated that after the airplane was raised
from the runway, all landing gears were in their
respective wheel wells with the doors fully closed.
He then entered the cockpit, noted the landing gear
motor circuit breaker was popped, and cycled the
landing gear selector handle from the down to the
up then down position. He then pushed in the landing
gear motor circuit breaker, turned on the master
switch, and the landing gear extended. The airplane
was then towed to the hangar.
Following recovery of the airplane, it was placed
on jacks and in the presence of an FAA airworthiness
inspector, six complete landing gear retraction
checks were performed with no discrepancies noted.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The failure of the pilot to verify the landing gear
was extended prior to touchdown resulting in a gear-up
landing.
Source: NTSB
Aircraft: Beech A36
Where: Santa Monica, CA
Injuries: 2 fatal
Phase of Flight: Takeoff
A Beech A36 was ditched into the ocean following a loss of engine power after departure from Santa Monica Municipal Airport, Santa Monica, California. The instrument rated private pilot, who was also a registered co-owner of the airplane, was operating it under the provisions of 14 CFR Part 91. The pilot and one passenger sustained fatal injuries; a third occupant listed on the instrument flight plan was not located. The airplane was destroyed. The pilot was destined for Brown Field Municipal Airport, San Diego, California to pick up a passenger and intended to return to Santa Monica later that day. Visual meteorological conditions prevailed and an instrument flight plan was in effect.
The airplane impacted the water off of Santa Monica beach approximately 2.5 statute miles west-southwest of the Santa Monica Airport and about 250 yards off shore. It was submerged in 20 feet of water. The pilot and one occupant were recovered from the airplane. Searches for the third occupant continued but were unsuccessful. Acquaintances of the pilot were unaware of who the third person would have been and at the time of this report, there was no additional information of a third person onboard the airplane.
According to the co-owner of the airplane, he and the pilot normally kept the utility doors locked when there were no aft seat passengers. They also agreed that when ditching the airplane, the cabin door would be unlatched prior to impact with the water. Initial responders reported that the cabin door was unlatched and that the utility doors were locked.
Witness Information
A lifeguard reported that he was 1 mile north of the airplane when he saw it at 400 feet above water level. It appeared to be at lower than normal altitude for airplanes flying in the area and continued a descent toward the ocean. The flight path of the airplane was toward Santa Monica airport from the southwest to the northeast. The lifeguard stated that the pilot appeared to be in control of the airplane and that from the time he first noticed the airplane until its impact with the water, approximately 5 seconds had gone by.
An additional witness was on the beach and took photos of the airplane as it approached the water. The photos show the airplane in a level flight attitude descent, approaching the beach from the west with the landing gear retracted. As the airplane impacted the water, it was in an upright attitude and moving in an easterly direction toward the beach. Upon impact, the airplane turned to a west-southwest heading on the surface of the water, and subsequently sank.
Personnel Information
The pilot held a private pilot certificate for single-engine airplanes with an instrument rating. He was issued a third class medical certificate with the restriction that he must wear corrective lenses during flight.
Copies of the pilot's personal flight logbook were obtained from his family. The total flight time logged was 428.4 hours. The pilot obtained his instrument rating in the accident airplane, which equated to his most recent flight review. The pilot logged 70.6 hours in the last 12 months, 15 hours in the last 6 months, and 2.2 hours in the past 30 days.
Pilot Information
According to Angel Flight personnel, the pilot had volunteered his time and airplane services to assist in the transport of a medical patient from San Diego to the Los Angeles area. The pilot was on the initial leg of the trip to pick up the patient when the accident occurred. The pilot received an Angel Flight checkout and the accident flight was his first mission.
Maintenance Information
An engine logbook entry showed that the engine was overhauled at a total time of 1,775 hours. The engine was field overhauled; there was no tachometer time noted in the maintenance entry. The connecting rod bearings and bushings, and the associated nuts and bolts, were replaced during this overhaul. Following the overhaul, mineral oil was installed in the engine. The engine was placed into storage.
An engine logbook entry indicated, in part, "Due to the long period of storage, it was disassembled, cleaned, inspected, and reassembled in accordance with the TCM IO-520 Overhaul manual, applicable Service Bulletins, and Airworthiness Directives." The engine was reinstalled on the airplane at a tachometer time of 2,819.89 hours.
An annual inspection was performed on the airplane. The tachometer time for the airplane was 3,321.61, and the time since major overhaul (TSMOH) of the engine was 502.72. The logbook entry indicated that all six cylinders were removed due to a blow by condition.
The aviation maintenance technician (AMT) that performed the annual inspection was interviewed. At the time of the annual inspection, the pilot was employed part-time at Corporate Jet Support, Hayward, California, about 5 hours per day. He worked full-time as a Production Supervisor for American Airlines, approximately 8 hours per day.
The AMT performed two annual inspections on the airplane. The AMT noted that during the inspection, the engine was removed from the airplane because the cylinders had to be removed. The exhaust and intake tubes were detached and the cylinders were pulled, as well as the pistons. The connecting rods were not removed. The cylinders were removed due to a blow by condition that was causing low compression. After the cylinders were repaired, they were reinstalled and the engine operated normally.
Wreckage and Impact Information
The airplane impacted offshore of the Santa Monica beach. Divers assisted in the recovery of the airplane that was floated to the surface, and pulled ashore. During the airplane recovery from the water, the cabin door departed from the rest of the structure and was not recovered.
Medical and Pathological Information
The Los Angeles County Coroner completed autopsies on the pilot and passenger. The cause of death for both occupants was attributed to drowning with complications from blunt force trauma. The FAA Bioaeronautical Research Laboratory performed toxicology testing on specimens of the pilot and passenger. Refer to the toxicology reports (contained in the public docket) for specific test parameters and results.
Survival Aspects
The airframe and seats were examined. The throw-over control yoke was positioned to the left side of the cockpit. The airplane was equipped with six seats which were outfitted with lap seatbelts. The two rearmost seats were stowed (latched up). The rear seats had lap belts that had airframe manufacturer identification tags sewn onto the belt material. The center and front seat lap seatbelts had no identification tags. Investigators examined the center and forward seatbelts. There was no visible evidence of webbing stretch or separated threads. The forward seats moved fore and aft on the seat tracks and would lock in position. The forward seats were removed and no deformation was evident to the seats or seat pans. The cockpit area remained intact and crushing was evident on the right and left fuselage sidewalls in the areas over the wing front spar. The cabin door latch bolt receivers on the fuselage were undamaged. The cabin emergency windows were found in the closed position. According to the aircraft manufacturer, the emergency windows opened normally when activated.
The Teledyne Continental IO-520-BA engine was examined. Both magnetos were severed from their attachment flanges on the engine and resting on the top of the engine casing, which had a hole that stretched from the top cylinder base nuts of cylinders 1 and 2, approximately 8 inches across and 6 inches wide at its widest section fore and aft.
The number 2 cylinder connecting rod was visible through the hole and portions of it and the connecting rod cap were fractured from the rod end. A 2.5-inch portion of the connecting rod from the crankshaft end contained the top portion of an attachment bolt and was located loose in the engine, just below the connecting rod. Two sections of bearing were peened and bent; one was located within the engine and one was located on the outside of the engine, between cylinders number 1 and 3. A bottom section of the cap bolt was also located between cylinders number 1 and 3 as well as a fractured and deformed portion of a castellated nut. A 1.25-inch section of rod cap was identified between the two cylinders. The other castellated nut was located between cylinders number 1 and 3, outside of the engine. It was fractured at one end and twisted.
The oil pan was removed and investigators noted sand in the pan. The sand was strained through a sieve and a 2.0-inch section of rod cap and both top and bottom bolt sections were identified. A 0.25-inch piece of castellated nut was also identified. Following the removal of the oil pan, investigators noted a hole in the bottom of the engine case, in alignment with the number 2 cylinder connecting rod above. The number 2 cylinder connecting rod was still attached to the piston by the piston pin. Upon initial examination, there were no signs of heat distress on the connecting rod and rod cap pieces or upon borescope inspection of the engine through the damaged case hole.
The engine was disassembled at Teledyne Continental Motors (TCM), Mobile, Alabama. The NTSB investigator and representatives from TCM and Raytheon Aircraft Company were present. After the engine was disassembled, the components were examined. The crankshaft was removed with the connecting rods (excluding the number 2 connecting rod) still attached. The cotter pins were removed from the castellated nuts, the torque values and lengths were measured and all values, excluding the upper and lower torque values for the number 1 connecting rod hardware (399 and 307 inch-pounds) and the upper torque value for the number 3 connecting rod hardware (467 inch-pounds), were within the manufacturer's specified limits of 475- 525 inch pounds. Investigators noted that the area surrounding the number 1 connecting rod appeared battered.
Materials Laboratory Report
The number 2 connecting rod, cap, bearings, bolts, nuts, and metal slivers from the engine were submitted to the NTSB Materials Laboratory for further examination. The cap and one arm of the connecting rod were fractured, both bolts and nuts were fractured and separated and the bearing was highly distorted. The assembly orientations were found by fracture matching the bolts and by aligning the bearing anti-rotation slots on the connecting rod pieces. One of the bolts had more damaged threads than the other, and one nut had a greater amount of deformation and fractures than the other nut
The connecting rod was fractured through the cap and one arm of the yoke. Magnified visual examinations of the fracture surfaces and surrounding areas revealed features such as surface topography and deformation patterns, which according to the metallurgist, was indicative of bending overstress separation at both fractures. No indications of preexisting cracking were found.
The fractured bolt from the numbered side of the connecting rod, was fractured through the grip slightly outboard of the rod split line. Although heavily damaged by post separation and mechanical contact, the fracture contained features and deformation patterns, according to the metallurgist, indicative of an overstress separation with no indications of preexisting cracking. The majority of the bolt threads were heavily deformed and distorted with the thread crest flattened toward the centerline of the bolt and lipped over on both sides of the thread flank, as if they were radially contacted and smashed. One region of the threads was sheared on one side of the bolt and no remnants of the cotter pin were found in the holes.
The bore of the mating bolt hole in the connecting rod arm showed significant axial scraping and damage. The metallurgist stated that the scraping and damage appeared consistent with contact by the bolt threads.
The bolt from the unnumbered side of the connecting rod had its head portion trapped in the deformed rod cap piece. The head was not removed. The metallurgist stated that the bolt was fractured just outboard of the split line and contained features typical of an overstress separation. The bolt threads were locally damaged and deformed but no threads were sheared. No remnants of the cotter pin were found in the holes.
Nut A was fractured in two pieces. It was heavily distorted and fractured in two places. The nut fractures were heavily damaged obscuring many of the features. The metallurgist stated that the undamaged fracture regions appeared typical of overstress separations. Although locally damaged, the internal threads were generally intact and not fractured or sheared. Contact patterns were apparent on the pressure flanks of the nut threads, consistent with prior full engagement with mating threads. The nut pieces had at least two smoothly curved deformation areas that approximated the major diameter of the bolt threads.
Nut B was fractured at one location at a cotter pin slot. The exterior of the nut was locally damaged in several areas including a severe dent in the washer face adjacent to the fracture. Contact patterns were apparent on the pressure flanks of the nut threads consistent with prior full engagement with mating threads. The majority of the internal nut threads were sheared as if the nut were pulled off the bolt. However, small regions that contained about 4 threads were not fractured. Four of these regions of intact threads were found evenly distributed around the inner diameter of the nut. The size and relative orientations of these regions matched the size and spacing of the cotter pin holes in the bolt. Additionally, the two threads furthest from the washer face were not sheared. According to the metallurgist, the pattern of intact threads indicates that at the time of shearing, the nut was rotated in the loosening direction approximately 4 threads from a position that would allow a cotter pin to be inserted through a hole in the bolt and slots in the nut.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The failure of an aviation maintenance technician to properly torque and cotter pin the number 2 connecting rod bolts at their attach point to the crankshaft, which resulted in the separation of the connecting rod in flight, and complete power loss.
Aircraft:
Beech B36TC
Where: San Diego, California
Injuries: None
Phase of Flight: Landing
A Beech B36TC overran the runway during the landing
roll at Montgomery Field Airport (MYF), San Diego,
California. The aircraft is operated under the provisions of 14 CFR Part
91. The commercial pilot, the sole occupant, was
not injured; the airplane sustained substantial
damage. The personal cross-country flight departed
the Big Bear City Airport (L35), Big Bear City,
California, about 1530, with San Diego as the final
destination. Visual meteorological conditions prevailed,
and an instrument flight rules (IFR) flight plan
had been filed.
In a written statement, the pilot reported that
she was cleared for the instrument landing system
(ILS) approach to MYF, circle to land runway 10R.
The airplane landed long, and the pilot applied
brakes upon touchdown. The left main tire blew out
and the pilot attempted a go-around. The airplane
overran the runway and veered to the left, resulting
in the left wing colliding with a runway end identifier
light. The airplane continued to the left and encountered
a ditch filled with soft mud. The pilot did not
report any mechanical problems with the airplane
prior to the accident.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's misjudged speed and altitude, which
led to a failure to attain the proper touchdown
point and a subsequent runway overrun. Also causal
was the pilot's delayed decision to perform a go-around.
Source: NTSB
Aircraft:
Beech BE-36A
Where:Mount Airy,
NC
Injuries: 4 fatal
Phase of Flight: Takeoff
At 1930 eastern standard time, a Beech BE-36A
registered to and operated by the commercial pilot,
collided with terrain shortly after takeoff from
the Mount Airy/Surry County Airport in Mount Airy,
North Carolina. The personal flight was operated
under the provisions of Title 14 CFR Part 91 and
instrument flight rules (IFR). Instrument meteorological
conditions prevailed, and an instrument flight plan
was filed. The pilot and four passengers received
fatal injuries, and the airplane was destroyed.
The airport manager stated that he had watched
the pilot load the airplane, and he heard the pilot
file an IFR flight plan in the airport lobby for
a flight to the Curtis L. Brown, Jr. Field identifier
4W1, located in Elizabethtown, North Carolina. The
manager stated that the pilot reported he was expecting
an 800-foot ceiling and 2 statute miles visibility
at arrival in Elizabethtown. After the airplane
was loaded, the airport manager noted that the Elizabethtown
Automated Weather Observation System (AWOS) readout
was reporting the ceiling was 500 feet broken, 1,800
feet overcast, and 2 statute miles visibility in
light drizzling rain. The airport manager heard
the airplane takeoff from runway 18, and he stated
that the engine sounded normal. Shortly after the
takeoff, the airport manager said he received a
telephone call from a local resident who stated
that she had heard an airplane making a "flapping"
sound followed by the sound of a crash. The airport
manager stated that he notified the local authorities,
who then initiated a search from the resident's
home. He said the airplane was quickly located near
the resident who reported the accident.
PERSONAL INFORMATION
A review of information on file with the FAA Airman's
Certification Division, Oklahoma City, Oklahoma,
revealed the pilot was issued a commercial pilot
certificate with ratings for airplane single and
multiengine land, and instrument airplane. A review
of records on file with the FAA Aero Medical Records
revealed the pilot held a second-class medical certificate
with no restrictions. The pilot reported on his
application for the medical certificate that he
had accumulated 475 total flight hours, and a review
of the pilot's logbook revealed that the pilot had
accumulated 712 total flight hours. The flight book
review also disclosed that the pilot had accumulated
44 hours of actual instrument flying, 3 hours of
actual instrument flying within the last 90-days.
AIRCRAFT INFORMATION
A review of maintenance records revealed that the
last recorded total time for the airframe was during
the annual inspection of 4,852.53 hours, and an
engine total time of 205.1 since factory overhaul.
The tachometer time and hobs meter was damaged and
the current airframe times could not be recovered.
Refueling records on file at Mount Airy-Surry County
Airport, Mount Airy, North Carolina, revealed that
the airplane was topped off with 26.4 gallons of
fuel. The engine logbooks revealed that the factory-overhauled
engine was equipped with a Shadin fuel flow indicating
system installed under STC-SA449GL.
METEOROLOGICAL INFORMATION
Mount Airy Automated Surface Observation at 1920,
wind calm, visibility two statue miles, drizzle,
ceiling overcast 500 feet, temperature eight degrees
Celsius, dew point six degrees Celsius, altimeter
30.00 inches of mercury. Instrument meteorological
conditions prevailed at the time of the accident.
According to local law enforcement Surry County
Sheriff Department and ground search teams, the
visibility in the vicinity of the crash scene was
very low with fog.
WRECKAGE AND IMPACT INFORMATION
Examination of the wreckage site found that the
airplane had collided with terrain on the south
side of an east-west oriented hill, in a near vertical
nose-down attitude. The engine and forward cabin
had penetrated the ground to a depth of about eight
feet. The wing leading edges had collapsed rearward,
and were compressed flat to the front wing spars.
The top and bottom wing panel skins were symmetrically
ballooned outward, exposing the wing internal structure.
The flap and aileron control surfaces remained loosely
attached to the wings. The rear cabin and rear fuselage
displayed accordion crush damage. The empennage
was found lying partially on top of the fuselage
structure and on the hillside. The top of the airplane
and empennage were on a northerly heading towards
the airport. Flight control continuity could not
be verified, however flight control components were
examined, and no anomalies were noted. It was found
during the recovery of the airplane that the landing
gear was retracted, flaps retracted, and that the
nose trim tab was set to 10 degrees trailing edge
down.
The fuel selector was found positioned on the
right main wing tank. The electric fuel boost pump
system had been modified to a boost pump that could
be selected to either LOW or ON (High). The cabin
door and the two utility baggage doors were separated
from the airplane. Both utility doors had separated
from their hinges and had fragmented into multiple
pieces.
The instrument panel was damaged, and the engine
and flight instruments were dislodged from the normally
install positions. The lower instrument panel switches
were deformed or missing. The King 200 (2-axis)
autopilot enunciator panel was not located. The
airplane was equipped with an auxiliary electric-driven
instrument air pump mounted on the firewall. The
artificial horizon was disassembled. There was scoring
present on the gyro mechanism.
The engine was a Teledyne Continental Motors
IO-550. Examination of the engine and accessory
components revealed the following. The engine and
propeller were located 8 feet below ground level
at the accident site. The engine remained partially
attached to the firewall by control cables, wiring
and hoses. The engine driven fuel pump, alternator,
air conditioner compressor, outboard portions of
the propeller governor and the starter were separated
from the engine. Both magnetos separated from their
mounting flanges and were resting on the top of
the engine. A small amount of fuel was found in
the separated engine driven fuel pump at the accident
site. The cooling fins on the Number 5 and 6 cylinders
revealed heavy impact damage on the top and forward
facing portions. The number 5 and 6 valve covers
were found broken. All six cylinders remained attached
to the engine case. The engine was moved to a storage
facility in Mount Airy, North Carolina for a post
recovery disassembly and examination. The engine
was rinsed prior to the post-recovery examination
to remove mud and soil from the engine.
The engine driven fuel pump was broken off of
the engine at its attachment flange. The lead seal
and safety wire was found intact. All fuel lines
to and from the fuel pump were fractured at the
fuel pump fittings. The fuel pump drive coupler
was found fractured at mid-span with the pump end
remaining in the fuel pump. Some fuel was found
in the engine driven fuel pump. The throttle arm
remained attached to the throttle body at the throttle
shaft and was separated from the throttle cable
attachment end. The throttle shaft was bent and
the throttle arm was partially disengaged. The fuel
metering unit mixture arm was found bent and resting
against the full rich stop. The fuel distribution
manifold fuel screen was found clean and free of
particles. The plunger moved up and down with spring
tension noted and the diaphragm was found intact.
The wiring harness was found impact damaged and
was cut by impact forces in numerous locations.
Both magnetos were impact damaged and contained
some mud in the internal mechanisms. Both impulse
couplers actuated during hand rotation. No spark
was produced from either magneto during hand rotation.
The number 1,2,3,4 and 6 top spark plugs and the
number 1,2,3,4, and 5 bottom spark plugs were removed
and appeared "normal" when compared to the Champion
Aviation Check-a Plug index. The number 5 top and
number 6 bottom spark plugs were impact damaged
and were not removed for inspection.
The number 5 cylinder sustained heavy impact
damage. The number 5 intake valve retainer halves
were found displaced slightly outward from the normal
position. The number 5 intake push-rod tubes were
found bent upward and aft, and were removed from
the engine prior to hand rotation of the crankshaft.
The engine was rotated by hand utilizing the fuel
pump drive coupler fitting on the aft end of the
crankshaft. Continuity to the engine camshaft, engine
driven accessories and to the front end of the crankshaft
was established during rotation. The engine crankshaft
was separated at the propeller flange, which remained
attached to the propeller.
The propeller was a three-bladed McCauley propeller.
One propeller blade had separated from the propeller
hub, and one blade was loose in the hub. All three-pitch
change knobs separated from their respective blades.
The two blades that remained attached to the propeller
hub were bent aft eight to 12 inches out from the
hub. All three blades tips were bent forward and
partially separated. Blade face polishing was minimal.
The spinner was crushed around the structure of
the hub.
MEDICAL AND PATHOLOGICAL
INFORMATION
The Office of the Chief Medical Examiner, Chapel
Hill, North Carolina, conducted a postmortem examination
of the pilot. The reported cause of death was "massive
blunt force injury". The forensic Toxicology Research
Section, Federal Aviation Administration, Oklahoma
City, Oklahoma performed postmortem toxicology of
specimens from the pilot. Carbon Monoxide and Cyanide
testing was not performed. No Ethanol was detected
in the urine. The following drugs were identified;
Paroxetine was detected in the Liver 4.912 (ug/mL,
ug/g), Paroxetine was also detected in the urine
0.141 (ug/mL, ug/g), Doxylamine was detected in
the Liver, Dextromethorphan was present in the Liver,
Dextrorphan was detected in the Lever, Dextrorphan
was also detected in the kidney, Pseudoephedrine
was detected in the Liver, Phenylpropanolamine was
detected in the Lever, and Acetaminophen was detected
in the Urine 16.82 (ug/ml, ug/g).
ADDITIONAL INFORMATION
A review of voice transcripts provided by the FAA
Raleigh (RDU) Automated Flight Service Station (AFSS)
found the pilot contacted the RDU AFSS on four separated
occasions requested weather information. He was
provided an outlook briefing for a flight from Mount
Airy (MWK) North Carolina to Elizabethtown (EYF),
North Carolina. These outlook briefings occurred
at 1737 Coordinated Universal Time (UTC) 2010 UTC,
2029 UTC, and 2324 UTC at which time he filed an
IFR flight plan from Mount Airy, North Carolina
to Elizabethtown, North Carolina with an Alternate
of Fayetteville (FAY) North Carolina.
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain control of the aircraft
due to spatial disorientation. A factor was low
clouds.
Source: NTSB
Aircraft:
Beech D-45
Where: Minden, LA
Injuries:2 Fatal
Phase of Flight: Go-around
The airplane impacted wooded terrain west of
the runway following an uncontrolled descent from
a go-around from runway 01. Strong gusty winds (15
to 25 knots) from the east prevailed at the airport
at the time of the accident. The private pilot,
who occupied the front seat, had accumulated a total
of 1,012.3 hours in the accident airplane. The pilot
rated passenger, who occupied the aft seat, had
accumulated a total of 321.5 hours, with none in
the accident airplane.
Review of the private pilot's personal and FAA
medical records indicated that he had an essential
tremor, a condition that caused his head and hands
to shake noticeably, and not associated with any
other disease. He continued to have progressive
symptoms even on medications. He had an episode
of unusual behavior, possibly related to his medications,
in 1996 which occurred during operation of an aircraft.
At the time of the accident, the private pilot was
on fairly large doses of diazepam and propanolol
to treat his essential tremor, medications which
he did not note on his most recent application for
a medical certificate. The FAA medical records indicated
that the FAA did not consider the private pilot
medically qualified in 1996 and in 2000.
Toxicological tests for the private pilot were
positive for diazepam (0.393 ug/ml) and its metabolites
in blood and for propanolol in the blood and liver.
Diazepam and its metabolites have substantial adverse
effects on judgment, alertness, and performance.
The pilot, in fact, complained of sedation from
the diazepam, and adverse performance effects would
be expected at the levels used. Propanolol which
lowers blood pressure and reduces heart rate response
to stress, may result in dizziness, fatigue, and
decreased G-tolerance, particularly at high doses.
The private pilot was impaired from the diazepam,
possibly from propanolol, and possibly from his
essential tremor.
No evidence of uncorrected discrepancies was
found in the maintenance records. No evidence of
an in-flight mechanical and/or flight control malfunction
was found that would have rendered the airplane
uncontrollable prior to the impact.
THE CAUSE
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The private pilot's failure to maintain aircraft
control during a go-around. Contributing factors
were the private pilot's impairment due to drugs,
the pilot-rated passenger's lack of experience in
the airplane, and the prevailing gusty crosswind
conditions.
Source: National Transportation
Board
Aircraft: Beech 65
Where: Lawrenceville, GA
Injuries: 1 fatal, 3 minor
Phase of flight: Takeoff
During the preflight inspection, some water was present in the fuel sample; it was drained until a clear sample was observed. Subsequently, the fuel tanks were topped off, and the remaining preflight inspection revealed no other anomalies. The pilot initiated a takeoff and upon reaching rotation speed, the airplane became airborne and the landing gear was retracted. The right engine immediately lost power, and the pilot feathered the engine and attempted to return to the airport. Shortly thereafter, the left engine lost power. The pilot informed the air traffic controller that the airplane had lost all power. The airplane subsequently collided with trees and terrain and a post crash fire ensued. A post-accident examination of the airframe and engine revealed no mechanical malfunctions or failures that would have precluded normal operation. Examination of fuel retrieved from the right main fuel tank, as well as fuel from the fixed base operator, revealed no anomalies. The left fuel selector valve was observed in the plugged port (no fluid flow) position, but it was most likely moved to that position during the accident sequence. The right fuel selector valve was partially aligned with the main fuel passageway and was unobstructed. The reason for the loss of engine power to both engines was not determined.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The failure of both engines for undetermined reasons.
Source: National Transportation Board
Aircraft:Beech
C90 King Air
Where:Dallas, TX
Injuries:1 Serious
Phase of Flight:Landing
HISTORY OF FLIGHT
A Beech C90 (King Air) twin-turboprop airplane was
substantially damaged when it impacted a residential
area during a forced landing following a loss of
engine power while on approach to the Dallas Love
Airport, Dallas, Texas. Private individuals, who
were in the process of purchasing the aircraft,
operated the airplane. The commercial pilot, who
was the sole occupant, sustained serious injuries.
Visual meteorological conditions prevailed and an
instrument flight rules flight plan was filed for
the 14 Code of Federal Regulations Part 91 business
flight. The cross-country flight originated from
Taos, New Mexico, at 1115 (2 hours and 7 minutes
prior to the accident).
According to reports from Dallas Love Air Traffic
Control Tower, the flight was on a visual approach
to runway 13L. When the airplane was on final approach,
the controller noticed the airplane in 'level flight
descending out of sight behind hangars.' The controller
asked the pilot if he was experiencing a problem;
however, the controller did not receive a reply.
The airplane descended into a residential area where
it struck power lines, a tree, a natural gas meter,
two private residences, and a fence.
According to an FAA inspector, who responded
to the accident site, the flight departed from Dallas
Love Airport at 0757 on the morning of the accident
after the pilot had the fuel tanks topped off with
244 gallons of fuel. Air traffic control data indicated
that the airplane descended from radar coverage
into Taos at 1044 (2 hours and 47 minutes after
departure). According to service personnel in Taos,
the airplane was on the ground for approximately
15 minutes, and departed for Dallas with just the
pilot on board.
An FAA inspector, who interviewed the pilot,
stated that the pilot reported that while the airplane
was on base leg to runway 13L at Dallas Love, the
right engine began to surge. The pilot turned on
the boost pumps and retracted the landing gear.
The pilot reported that the right engine lost total
power and the airplane's airspeed was approaching
the minimum controllable airspeed (Vmc); therefore,
he reduced power on the left engine and attempted
a forced landing to the residential area.
In a written statement, submitted to the NTSB
investigator-in-charge (IIC), the pilot reported
that the return flight from Taos was uneventful
until the flight approached Wichita Falls, Texas,
when the pilot noticed that the right hand fuel
gauge 'spiked to zero and returned to its previous
indication.' The pilot reported that the 'anomaly
happened twice and did not occur again for the remainder
of the flight.' He added that the flight continued
'normally' until the airplane turned onto short
final for runway 13L. The right engine 'began to
surge violently, so [he] brought the power back
and increased power to the left engine. This made
the airplane aircraft roll to the right, so [he]
brought [the left] engine back as well.' The pilot
realized that the airplane would not make it to
the runway and he looked for a place to land. The
pilot found an alley in a residential area and attempted
to land there. He stated that the airplane was about
to impact the power lines, so he 'retracted the
landing gear, brought the condition levers back
to cut-off, and kept flying until [he] blacked out.'
One witness, who was located in the residential
area, stated that she heard a 'crackling sound,'
which caused her to look up and see the airplane
'barely hitting the electric tower. The motor wasn't
on.' She added that one of the wings clipped a television
satellite dish and the side of a house. The aircraft
continued across the street and impacted a garage
and a tree where it came to rest.
Another witness, who was also located in the
residential area, stated that he noticed the airplane
flying very low. He observed the airplane impact
electrical wires with the lower left wing and 'sparks
flew everywhere.' The airplane then disappeared
from his view. He added that he thought the 'engines
were missing or sputtering.'
PERSONNEL INFORMATION
The commercial pilot held a second-class medical
certificate without limitations. The pilot reported
having accumulated approximately 7,000 total flight
hours, of which 5,000 hours were in multi-engine
airplanes and 100 hours were in the same make and
model as the accident airplane.
AIRCRAFT INFORMATION
The aircraft was equipped with two 550 shaft-horsepower
Pratt & Whitney PT6A-21 engines. Review of maintenance
records revealed that the aircraft underwent Phase
2 and Phase 3 inspections in accordance with the
Beech King Air inspection procedures on April 27,
2001, at an aircraft total time of 7,325.2 hours.
At the time of the last inspection, the engines
had accumulated a total of 7,325.2 hours, and had
accumulated 3,892.2 and 3,669.8 hours since the
last overhaul on the left and right engines, respectively.
The left and right engines had accumulated 1,405.2
and 1,182.8 hours since their last hot section inspections,
respectively. During the aircraft's last inspection,
McCauley 4-bladed propellers were installed in accordance
with Supplemental Type Certificate (STC) SA1241GL
at propeller total times of 50.8 hours for both
the left and right propellers. At the time of the
accident, the airplane had accumulated a total of
7,356 hours.
According to the King Air C90 Pilot Operating
Handbook fuel system description, 'the fuel system
consists of two separate systems connected by a
crossfeed system. Fuel for each engine is supplied
from a nacelle tank and four interconnected wing
tanks for a total of 192 gallons of usable fuel
for each side with all tanks full. The outboard
wing tanks supply the center section wing tank by
gravity flow. The nacelle tank draws its fuel supply
from the center section tank. Since the center section
tank is lower than the other wing tanks and the
nacelle tank, the fuel is transferred to the nacelle
tank by the fuel transfer pump in the low spot of
the center section tank. Each system has two filler
openings, one in the nacelle tank and one in the
leading edge tank. To assure that the system is
properly filled, service the nacelle tank first,
then the wing tanks.'
In written statements provided by the fueling
service in Dallas, the aircraft refueling personnel,
who fueled the airplane on the morning of the accident,
stated that they filled the nacelle fuel tanks prior
to filling the wing fuel tanks.
WRECKAGE AND IMPACT INFORMATION
The airplane came to rest upright in the yard of
a residence. A tree was crushed under the belly
of the aircraft. Review of photographs taken at
the accident site revealed that the airplane's wings,
outboard of both engines, sustained impact damage,
which compromised the fuel system. The propellers
remained attached to the engines. The left and right
propeller blades were intact and attached to the
propeller hubs and were bent and twisted. The engines
remained attached to their wings; however, they
were deflected downward. The left horizontal stabilizer
was torn from its attachment fitting.
Cockpit documentation revealed that the fuel
boost and transfer pumps were in the OFF position,
the power levers were in the mid-range position,
the propeller levers were in the full forward position,
and the condition levers were at the low idle position.
The rudder trim was set in the neutral position,
the aileron trim was found in the maximum (5 degrees)
right wing down trim, and the elevator trim was
set at a 7 degree up position.
TESTS AND RESEARCH
An environmental inspector with the City of Dallas'
Storm Water Quality department conducted a petroleum
risk test. According to the inspector, upon his
arrival at the accident site, he noticed the 'fire
department spraying fire-suppressing [foam] around
plane wreckage. Water runoff from related activities
showed no signs of any petroleum product. No rainbow
sheen or fuel odor was noted on and in water. A
test of runoff with 'Spilfyter' (brand) chemical
classifier showed negative results for petroleum
risk with pH normal at neutral.' The inspector returned
to the accident site the following day and conducted
the same tests and 'found no signs of fuel in street,
curb, or storm drain system.'
An NTSB investigator and a representative of
the aircraft manufacturer examined the fuel lines
of the airplane at Air Salvage of Dallas, Lancaster,
Texas. According to the NTSB investigator, approximately
1 liter of fuel was drained from the left and right
fuel sumps located in the belly of the aircraft.
They then examined both the left and right engines
and noted that for each engine, there was no fuel
in the line between the firewall to the fuel heater,
nor was there fuel in the line between the fuel
pump and the fuel control unit.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The pilot's failure to refuel the airplane,
which resulted in fuel exhaustion and subsequent
loss of dual engine power while on approach.
Source: National Transportation
Safety Board
Aircraft:Beech
Travel Air
Where:Dunbar, WI
Injuries:I fatal
Phase of Flight:Instrument
approach
A Beech D-95A Travelair was destroyed when it impacted the
ground near Dunbar, Wisconsin. The impact site was
approximately eight miles south of Ford Airport
(IMT), Iron Mountain, Michigan. The 14 CFR Part
91 positioning flight had departed Huntsville International
Airport (HSV), Huntsville, Alabama, at 2339 on January
5, 2000, en route to Ford Airport. At 0337, the
pilot reported the airplane was established on the
final approach course on the ILS Rwy 01 approach
to Ford Airport. At 0338, the pilot reported moderate
rime icing at 3,200 feet mean sea level to Minneapolis
Center. There were no further communications with
the airplane. The airline transport pilot received
fatal injuries. Visual meteorological conditions
prevailed at IMT and an IFR flight plan had been
filed.
The operator reported that the pilot was notified
at approximately 1630 of a Part 135 flight for parts
delivery from IMT to HSV. The operator reported
the pilot obtained a weather briefing and filed
a flight plan prior to leaving home. The operator
reported the pilot departed for HSV at approximately
1730.
The pilot contacted the Green Bay, Wisconsin,
Automated Flight Service Station (AFSS) at 1648
for a pre-flight briefing and filed an IFR flight
plan from IMT to HSV. The takeoff time was listed
as 1710 with 4 hours 15 minutes en route at 160
nautical miles per hours. The estimated time at
arrival was 2125.
Minneapolis ARTCC reported the subject aircraft
departed IMT at 1732. HSV tower reported it arrived
at HSV at 2227.
The airplane was topped off with 94 gallons of
100 LL/Avgas. A lineman reported that he brought
the pilot something to eat from a local restaurant.
The lineman and mechanic reported the pilot was
cold, and that the pilot had informed them that
the airplane's heater had not worked since shortly
after takeoff. The mechanic reported that he and
the pilot went out to the airplane. The mechanic
drained about two spoonfuls of fuel out of the heater
drain bowl. The mechanic reported the pilot operationally
checked the heater and it "appeared to function
normal for the couple of minutes that he let it
run." The lineman reported that the pilot said he
would "stop somewhere and spend the night" if the
heater did not work on the return trip.
The pilot contacted the Anniston, Alabama, AFSS
at 2330 for a pre-flight briefing and filed an IFR
flight plan from HSV to IMT. The takeoff time was
listed as 2345 with 4 hours 15 minutes en route
at 160 nautical miles per hour. The estimated time
of arrival was 0400.
The HSV tower reported that the aircraft departed
HSV at 2339.
At 0257:29, the pilot contacted Minneapolis ARTCC
and reported he was at 9,000 feet mean sea level
(msl).
At 0257:50, the pilot reported he was, "... just
starting to pick up a little bit of ice here in
the tops. Do you have any reports up ahead of us
down below at all?"
At 0258:24, ATC cleared the pilot to descend
to 7,000 feet msl.
AT 0259:04, the pilot reported, "We just came
out on top again here at nine. Maybe we can stay
up here for a bit longer."
At 0259:09, ATC responded, "' maintain niner
thousand."
At 0324:19, the pilot reported, "'going ten degrees
left for the localizer."
At 0324:55, ATC reported, "' roger. You can report
established on the localizer. Change to my frequency
one two one point two five."
At 0325:03, the pilot reported, "We'll report
that, and, ah, we're on one twenty one and a quarter.'
At 0325:08, ATC reported, "' descend at pilot's
discretion. Maintain three thousand two hundred."
At 0325:14, the pilot reported, "Make that three
point two."
At 0334:34, the last radar contact indicated
the airplane was at 3,900 feet msl and on a heading
toward IMT which was approximately 22 nautical miles
to the north.
At 0336:37, ATC reported, "Radar contact is lost.
Are you established on the localizer?"
At 0336:42, the pilot responded, "Yes, sir, we
are and we're just getting some pretty good moderate
ice here at thirty two hundred."
At 0336:48, ATC reported, "Roger. Cleared for
the ILS Runway One approach to the Iron Mountain
airport. Before you leave my frequency, could you
tell me what type of icing you're getting and the
temperature?"
At 0336:59, the pilot responded, "It's rime,
sir, and we're at about, oh, it looks like about,
minus ten C."
At 0337:09, ATC reported, "Roger. Thank you sir.
And, change to advisory frequency approved. Cancellation
or down time this frequency."
At 0337:18, N5918S reported, "Back with you for
cancellation"
There were no further transmissions from the
aircraft.
A search was initiated for the aircraft and it
was located in a wooded area with rolling hills.
There were no witnesses to the accident.
PERSONNEL INFORMATION
The pilot was an airline transport rated pilot with
single and multi-engine land ratings, and a commercial
single engine sea rating. He was a Certified Flight
Instructor in single and multi-engine land airplanes,
and an instrument instructor. He held a Class 2
medical certificate. He had a total of about 10,000
hours of flight time. 4,600 hours were in multi-engine
airplanes, with about 400 hours in make and model.
The pilot was designated as Pilot in Command
(PIC) in the Beech D-95A on July 12, 1996. He had
also been designated as PIC in the following aircraft:
C-402, C-404, C-310, C-208, and C-441. His last
Part 135 check ride was in the C-414.
AIRCRAFT INFORMATION
The airplane was a twin engine Beech D-95A, Travel
Air. The airplane seated 4 and had a maximum gross
weight of 4,200 pounds. The engines were 180 horsepower
Lycoming IO-360-B1B engines. The airplane had flown
about 26 hours since the last inspection and had
a total time of about 8,924 hours.
The airplane was equipped with the following
de-ice/anti-ice equipment: propeller anti-ice, windshield
anti-ice, de-icing boots and heated pitot tube.
METEOROLOGICAL CONDITIONS
At 0254, the weather reported at IMT was: Ceiling
1,700 feet overcast; visibility 8 miles; temperature
-5 degrees C; dew point -7 degrees C; winds 180
degrees at 11 knots; altimeter setting 29.83 inches
of Hg.; snow ended 0207 began 0228 and ended 0241.
At 0315, the weather reported at IMT was: Ceiling
1,300 feet overcast; visibility 7 miles; temperature
-5 degrees C; dew point -6 degrees C; winds 170
degrees at 8 knots; altimeter setting 29.83 inches
of Hg.
At 0354, the weather reported at IMT was: Ceiling
1,100 feet overcast; visibility 6 miles, mist; temperature
-4 degrees C; dew point -6 degrees C; winds 180
degrees at 8 knots; altimeter setting 29.81 inches
of Hg.
The following AIRMETs were issued by the Aviation
Weather Advisory Center (AWC) in Kansas City, Missouri
:
AIRMET Sierra Update 1 for IFR reported occasional
ceilings/visibilities below 1,000 feet / 3 miles
in clouds... precipitation and mist. Conditions
moving eastward during the period...continuing beyond
0900 through 1500. The area encompassed by this
AIRMET included the accident site.
AIRMET Tango Update 1 for Turbulence reported
occasional moderate turbulence below 6,000 feet
due to occasional strong and gusty low level flow
across the area. Conditions continuing beyond 0900
through 1600. The area encompassed by this AIRMET
included the accident site.
AIRMET Zulu Update 1 for Ice reported occasional
moderate rime or mixed icing in cloud and in precipitation
below 10,000 feet. Conditions continuing beyond
0900 through 1500. Freezing Level... Surface to
4,000 feet for an area that included the accident
location. The area encompassed by this AIRMET included
the accident site.
AIDS TO NAVIGATION
The IMT ILS Rwy 1 instrument approach plate indicates
that the Final Approach Fix (FAF) for the localizer
approach is 5.0 nautical miles from the runway.
The ILS glideslope intercept altitude is 2,900 feet
msl. The altitude of the glideslope over the FAF
is 2,804 feet msl. The inbound heading is 010 degrees.
The IMT airport elevation is 1,182 feet msl.
WRECKAGE AND IMPACT INFORMATION
The location of the main wreckage was about 7.8
nautical miles south of the IMT airport and at coordinates
45 degrees 41.5 minutes North, 88 degrees 8.2 minutes
West. The fuselage and cockpit were destroyed by
fire.
The wreckage path was on a heading of approximately
002 degrees. A tree about 60 feet in height and
about 370 feet from the main wreckage had its top
branches broken, and it appeared to be the initial
tree impacted by the airplane.
A broken branch with a diagonal cut that exhibited
a gray paint transfer was found under a tree about
60 feet from the initial impact.
The outboard left wing panel was separated outboard
of the left engine nacelle and was found along the
left side of the wreckage trail about 150 feet from
the initial tree impact.
A fragment of the crushed nose cone that exhibited
burn damage was found co-located with the left wing
panel.
The crushed nosecone was found lodged about 25
feet up in a tree that was about 200 feet from the
initial impact point. The fiberglass nosecone exhibited
crushing, tearing, and traces of smoke and burn
damage. The heater unit located just aft of the
nosecone of the airplane was found in the main wreckage.
The heater unit exhibited impact damage and traces
of smoke and burn damage.
The left stabilizer and elevator were found about
220 feet from the initial impact point. They were
separated from the empennage at a location near
the inboard end of the elevator. The elevator trim
tab was positioned beyond normal limits of travel.
The actuator mount was separated from the stabilizer.
The stabilizer exhibited crush damage along the
leading edge.
The right outboard wing panel was found about
250 feet from the initial impact point. It was separated
at a location near the inboard end of the aileron.
The adjacent inboard four-foot section of the right
wing panel was found about 350 feet from the initial
impact point. The fuel filler cap was found secured
within the fuel filler port.
The outboard three-quarters of the right elevator
and stabilizer were located next to the inboard
end of the right wing at the main wreckage site.
The main wreckage came to rest approximately
370 to 400 feet north of the initial impact. The
wreckage included the fuselage, inboard wings, vertical
stabilizer, and both engines. The fuselage was found
inverted with both engines still attached to their
respective engine mounts. The fuselage, cockpit,
and cabin area were destroyed by fire.
The right propeller was still attached to the
right engine crankshaft. The left propeller was
separated from the left engine crankshaft at a location
about two inches behind the propeller mount flange.
The left propeller was found in the ground under
the left engine.
The right landing gear was found in the extended
position. The right main landing gear door was nicked
along the front edge of the gear door. The left
main landing gear door had two impact nicks along
the front edge of the gear door. The nose landing
gear assembly was found in the extended position.
The cockpit instruments, flight controls, engine
controls and fuel tank selector controls were destroyed
by fire.
The elevator control cables were found to be
continuous from the cockpit aft to the elevator
bellcrank. One of the two rudder cables was found
separated with a broomstraw separation at a location
about four feet aft of the aft wing spar. The other
cable exhibited continuous continuity. The rudder
trim tab and elevator trim tabs were continuous
and were traced from the cockpit aft to a location
adjacent to the horizontal stabilizers.
The inspection of the left engine revealed continuity.
Thumb compression and suction were confirmed on
all cylinders. The left and right magnetos exhibited
internal fire damage and did not produce spark.
The engine driven fuel pump arm was cycled but no
suction or pressure was noted. The pump was opened
and fuel was found in the unit.
The vacuum pump drive was damaged by impact and
fire and would not rotate. The pump was opened and
the rotor and vanes were found intact.
The inspection of the right engine revealed continuity.
Thumb compression and suction were confirmed on
all cylinders. Fuel was observed coming out of the
engine driven fuel pump outlet port when the engine
was rotated. Both the left and right magnetos produced
spark.
The vacuum pump drive was rotated and suction
and pressure was noted from the ports. The pump
was opened and the rotor and vanes were found intact.
The left propeller assembly was separated from
the left engine crankshaft. The crankshaft fracture
surface exhibited a 45-degree lip along the circumference
of the crankshaft. Both propeller blades were missing
about 3 inches of their blade tips. Both blades
exhibited twist and nicks along the leading edges.
The right engine propeller assembly remained
attached to the right engine. It exhibited leading
edge nicking and aft curling of both blade tips.
The spinner on the right propeller exhibited about
45 degrees of torsional twisting.
MEDICAL AND PATHOLOGICAL
INFORMATION
A Forensic Toxicology Fatal Accident Report was
prepared by the FAA Civil Aeromedical Institute.
The report indicated the following results:
Carbon monoxide: Not performed.
Cyanide: Not performed.
No ethanol detected in kidney.
No ethanol detected in muscle.
No drugs detected in kidney.
ADDITIONAL INFORMATION
The official Weather Service definition of moderate
icing is: "The rate of accumulation is such that
even short encounters become potentially hazardous
and use of deicing/anti-icing equipment or diversion
is necessary."
According to the Beechcraft Safety Communique,
July 16, 1980, Travel Air D-95A's were CAR Part
3 type certificated airplanes which were approved
for flight into light to moderate icing conditions.
However, they were not approved for extended flight
in moderate icing conditions or any flights in any
severe icing condition.
The National Transportation Safety Board determines
the probable cause(s) of this accident/incident
as follows: The pilot failed to maintain a proper
glidepath and obstacle clearance during an instrument
approach. Additional factors to the accident included
the dark night, icing conditions, flight into known
adverse weather, and conditions conducive to pilot
fatigue.
Source: NTSB
Aircraft: Beech 95B55
Where: Clarion, IA
Injuries: 1 fatal
Phase of flight: Cruising
A Beech 95-B55 operated by a private pilot, was substantially damaged when it impacted the ground near Clarion, Iowa. The 14 Code of Federal Regulations Part 91 personal flight was operating in visual meteorological conditions without a flight plan. The pilot, who was the sole occupant, was fatally injured. The local flight originated from the Clarion Municipal Airport (CAV), Clarion, Iowa, about 1410.
The pilot's son reported that he spoke with the pilot prior to the accident. He said that his father told him he was planning to fly the accident airplane on a local flight.
A witness to the accident reported seeing the airplane flying northwest when it suddenly entered a counter-clockwise spinning dive toward the ground. The witness stated to a Federal Aviation Administration (FAA) inspector that the airplane made about four revolutions before impacting the ground.
The pilot held a private pilot certificate with single engine land, multiengine land, and instrument airplane ratings. The pilot held a third-class medical certificate. The medical certificate stated that the pilot must wear corrective lenses for near and distant vision, and use hearing amplification. According to flight instructor records, the pilot had received a flight review on May 10, 2010, in a single engine Piper PA-28-236. The pilot's flight logbook was not available for review; however, the pilot reported having 4,000 hours total flight experience on his most recent medical application.
The airplane was a Beechcraft model 95-B55. It was a twin-engine monoplane with predominately aluminum construction. It had a retractable tricycle landing gear, and could seat 6 occupants including the pilot. The airplane was powered by two Continental model IO-470-L engines, each rated to produce 260 horsepower.
The most recent maintenance logbook entry indicated that an annual inspection of the airframe was completed on July 1, 2007, at a total airframe time of 8,854 hours.
The most recent maintenance logbook entry, dated April 9, 2007, for the left engine indicated that all six cylinders were removed from the engine and replaced due to low compression. The maintenance entry indicated that the left engine was inspected in accordance with an annual inspection on that date.
The most recent maintenance logbook entry, dated April 9, 2007, for the right engine indicated that three cylinders were removed from the engine due to low compression. Those cylinders were honed, the affected pistons cleaned, and new piston rings installed. The maintenance entry indicated that the right engine was inspected in accordance with an annual inspection on that date.
No subsequent maintenance entries were found in the airframe, engine, or propeller logbooks.
The weather reporting station at CAV recorded the weather conditions at 1415 as: wind 340 degrees at 8 knots; 10 miles visibility; clear skies; temperature 13 degrees Celsius; dew point -3 degrees Celsius; altimeter setting 30.05 inches of mercury.
The airplane impacted a level field about 0.5 miles west of CAV. The aft fuselage was in a near vertical orientation when first responders arrived on scene. Federal Aviation Administration inspectors found the left engine magneto switch positioned to the "R" position. The switch for the right engine was positioned to "Both.” The switch assembly was broken loose from the airframe. The fuel flow indicator was broken loose from its mounting and the instrument lens was broken. The instrument face was bent and the indicator needles showed no fuel flow on the left engine and 12 gallons per hour fuel flow on the right engine. The left propeller control was found in an aft "feathered" position at the accident scene. There was significant crushing in the area of the engine controls and instrument panel.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's failure to maintain control of the airplane. Contributing to the accident was the loss of left engine power for undetermined reasons.
Aircraft:
Breezy
Where:Pell City, AL
Injuries:1 fatal
Phase of Flight:Low
passes
A Moore Sammie, M-Breezy, experimental airplane,
N9167C, registered to a private owner/operator,
collided with the ground after takeoff at Pell City
Airport, Alabama. The personal flight was operated
by the pilot under the provisions of Title 14 CFR
Part 91 with no flight plan filed. Visual meteorological
conditions prevailed at the time of the accident.
The airplane sustained substantial damage, and the
private pilot received fatal injuries.
According to witnesses, the airplane made several
low altitude passes along runway 20 with steep turn
maneuvers to reverse the direction. During the last
steep turn maneuver, the airplane began a downward
spin. The airplane continued this spiral until it
hit the ground. The spiral began approximately 300
feet above the ground. The witnesses pulled the
pilot from the wreckage, and began cardio pulmonary
resuscitation and first aid. They worked on the
pilot until the rescue personnel arrived.
A Lycoming 0-320, 180 horsepower engine, powered
the experimental airplane. Airplane logbooks were
not recovered for examination.
The pilot held a private pilot certificate with
an airplane single engine land rating. The pilot's
total flight time was approximately 1250 hours.
The pilot held a third class medical certificate
with no waivers or limitations.
The Anniston Metropolitan Airport 1753 weather
observation reported winds 160 at 9 knots with gusts
up to 15 knots, visibility 10 statute miles, temperature
23 degrees Celsius, and a dew point of 8 degrees
Celsius. There were few clouds at 6500 feet above
ground level with no ceiling. The altimeter was
30.19. Visual conditions prevailed at the time of
accident; conditions of light were dusk.
Examination of the wreckage site revealed the
airplane came to rest at the north end of runway
20. The airplane showed signs of crush damage. All
flight controls and flight surfaces were present
at the site. The pilot did not report any mechanical
or flight control malfunction prior to the accident.
The State Toxicology and Accident Research Laboratory
in Oklahoma City, Oklahoma performed the forensic
toxicology. The cause of death was head trauma.
THE CAUSE
The National Transportation Safety Board determines
the probable cause(s) of this accident as follows:
The pilot's failure to maintain flying speed, followed
by an inadvertent stall spin, and subsequent collision
with terrain.
Source: National Transportation
Board
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